Elevation Resources DAILY OPERATIONS. Feb MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368. RIG SUPERVISOR: Jimmy Nobles PBTD:

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1 FIELD: COUNTY/STATE: PMD: 17,368 PVD: 10,915 SURFACE LOCATION: BOTTOM HOLE LOCATION: ELEVATION (RKB): 3,143 Emma (Devonian) Andrews/Texas API #: PERMIT NUMBER: SPUD DATE & TIME: Mar DAYS FROM SPUD: 57 DAYS ON LOCATION: 63 WELL ENGINEER: OBJECTIVE: JOB NAME: CONTRACTOR/RIG#: 2600' FSL, 678' FWL, Blk 1, Sec. 24, UL Survey 1500' FNL, 500' FWL, Blk 1 Sec. 21, UL Survey Jason L. Kincaid Drill horizontal devonian under $3.8MM drilling costs Grassroots Horizontal Devonian Independence Contract Drilling/ICD/208 Elevation Resources DAILY OPERATIONS Feb MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 R/D ON UNIVERSITY 1-20 #3H & MIRU ON UNIVERSITY 1-24 UNIT 1H. MIRU ICD #208 ON UNIVERSITY 1-24 UNIT 1H. SOLID LIBERTY MOVED TRAILER, OFFICE, & WATER/SEPTIC SKIDS TO NEW LOCATION. AVEDA MOVED TOOLPUSHER TRAILER, LOOSE RIG EQUIP & TUBULARS TO NEW LOCATION. CONTINUE R/D ON UNIVERSITY 1-20 #3H. CONTINUE R/D & MIRU ON UNIVERSITY 1-24 UNIT 1H. Feb MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 R/D ON UNIVERSITY 1-20 #3H & MIRU ON UNIVERSITY 1-24 UNIT 1H. R/D ON UNIVERSITY 1-20 #3H & MIRU ON UNIVERSITY 1-24 UNIT 1H. HAD ELECTRICAL PROBEMS W/ DRWKS FOR ABOUT 6 HRS WHICH DELAYED GETTING THE DERRICK LAID DN UNTIL LATE AFTERNOON. ABOUT 75% OF BACK YARD IN PLACE ON NEW LOCATION. CONTINUE R/D & MIRU ON UNIVERSITY 1-24 UNIT 1H. INSTALL & TEST TUBING HEAD ON UNIVERSITY 1-20 #3H. Mar MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 R/D ON UNIVERSITY 1-20 #3H & MIRU ON UNIVERSITY 1-24 UNIT 1H. R/D ON UNIVERSITY 1-20 #3H & MIRU ON UNIVERSITY 1-24 UNIT 1H. ICY CONDITIONS. CAMERON SERVICE HAND UNABLE TO INSTALL TUBING HEAD ON UNIVERSITY 1-20 #3H DUE TO 7" SLIPS BEING SET ABOUT 1 1/2 INCHES HIGH IN THE WELLHEAD. CONTINUE MIRU ON UNIVERSITY 1-24 UNIT 1H. Mar MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 MIRU ON UNIVERSITY 1-24 UNIT 1H. MIRU ON UNIVERSITY 1-24 UNIT 1H. BACK YARD RIGGED UP & GROUNDED, SUB & DRILLER'S HOUSE RAISED, SCOPE OUT & R/U DERRICK, SET IN CRADLE READY TO BE RAISED. RAISE & R/U DERRICK & FLOOR. FILL PITS & MIX SPUD MUD. FUNCTION TEST EQUIP & PERFORM PRESPUD CHECK LIST. Mar MD: TVD: FOOTAGE: MW: 8.6 LB PTD: 17,368 RAISE DERRICK & R/U. REPAIR POWER LEAD TO TOP DRIVE. PERFORM PRESPUD CHECK LIST. MIX SPUD MUD. RAISE DERRICK. HANG TRACK, INSTALL TOP DRIVE, INSTALL STAND PIPE, MUD HOSE, & SERVICE LOOP. FILL MUD PITS W/ FW & MIX SPUD MUD. PROBLEMS GETTING TOP DRIVE POWERED UP. ELECTRICIANS HAD TO MAKE A SPLICE ON POWER LEAD. R/U FLOOR. HAD POWER TO TOP REPORT TIME, FUNCTION TESTING. FINISH FUNCTION TEST. INSTALL CONDUCTOR RISER & N/U FLOWLINE. P/U 17 1/2" BHA. SPUD WELL.

2 Mar MD: TVD: FOOTAGE: MW: 8.6 LB PTD: 17,368 RIG REPAIR. WORK ON TOP DRIVE. WHILE WORK ON TOP DRIVE CONTINUE TO PREP TO SPUD. RIG REPAIR. ELECTRICIANS WORK ON TOP DRIVE. INSTALLED NEW SERVICE LOOP. TOP DRIVE STILL NOT OPERATIONAL AS OF REPORT TIME. 24 HRS DOWNTIME. INSTALL DUMP LINE F/ SHAKERS TO RES PIT. CHANGE SHAKER SCREENS. FINISH MIXING SPUD MUD. UNLOAD 13 3/8" CASING. MOVE DC'S TO RACK & STRAP. WELD ON CONDUCTOR RISER. INFORM TRRC OF SPUD, CASING & CEMENT JOB. ASSIGNED JOB # REPAIR TOP DRIVE, P/U BHA & SPUD WELL. Mar MD: 144 TVD: 144 FOOTAGE: 144 MW: 8.6 LB PTD: 17,368 RIG REPAIR. ICD ELECTRICIANS WORK ON TOP DRIVE. P/U 17 1/2 BHA, RIH 105'. SPUD 0530 HRS 3/5/15. RIG REPAIR. ELECTRICIANS WORK ON TOP DRIVE.;INSTALL MOUSEHOLE & FINISH R/U FLOOR. P/U 7" DC'S & STAND DERRICK. P/U ONE STAND OF DRILL PIPE & STAND IN DERRICK TO USE F/ KELLY. ICY WEATHER CONDITIONS.;P/U 17 1/2 BHA & RIH. TAG 105'.;BREAK CIRC, REPAIR SEVERAL LEAKS. PROBLEM GETTING TRASH PUMP PRIMED ON CUTTINGS CHUTE. TOTCO STROKE COUNTER ON #2 & FLOW SHOW NOT WORKING. CALL F/ SERVICE. PREP TO SPUD.;SPUD UNIVERSITY 1-24 UNIT 0530 ON 3/5/15. SPUD W/ 250 GPM & GRADUALLY INCREASE W/ DEPTH. FW SPUD MUD 8.6 PPG 43 VIS. DRILL F/ 105' TO 144'. WOB 3-7K, TD 30 RPM, MOTOR 50 RPM, PP 350 PSI, TORQUE 1000 FT/LBS. DRILL 17 1/2" SURFACE HOLE. DROP GYRO & TOOH TO RUN CASING. Mar MD: 350 TVD: 350 FOOTAGE: 206 MW: 8.6 LB PTD: 17,368 DRILL 17 1/2" SURFACE HOLE F/ 144' TO 270'. FLOWLINE PACKED OFF. REMOVE, CLEAN OUT & REINSTALL. DRILL 270' TO 350'. DRILL 17 1/2" SURFACE HOLE F/ 144' TO 270'. WOB 5-10K, TD 40 RPM, 335 GPM, MOTOR 54 RPM, PP 400 PSI, TORQUE 3-6K FT/LBS. FLOWLINE, SHAKERS & CONDUCTOR PLUGGED UP.;UNPLUG FLOWLINE & SHAKERS. FLOW SHOW PADDLE COMPLETELY PACKED OFF W/ CLAY & GRAVEL, ALSO PACKED THE FLOWLINE OFF SOLID ALL THE WAY FROM FLOW SHOW TO THE CONDUCTOR. CLEAN OUT & REMOVE PADDLE. BREAK FLOWLINE APART & USE A LONG PIECE OF 1" POLY LINE TO PUNCH & WASH THRU PACKED OFF CLAY & GRAVEL. REMOVE FLOWLINE & PUT ON PIPE RACK IN ORDER TO GET IT CLEANED OUT. CALLED OUT WELDER & INSTALLED 2 MORE JET LINES.;START BACK DRILLING, CLAY & GRAVEL PLUGGING UP POSSUM BELLY & SHAKERS. PUMP SWEEP W/ SOAP. CONTINUE CONTROL DRILL SLOWLY & SHOVELING POSSUM BELLY. PUT SOAP STICKS IN PIPE ON CONNECTIONS. ADD SOME DRILLING SOAP TO ACTIVE. JETTED 05OO & 0530 TO CLEAR CUTTINGS. DRILL F/ 270' TO 350'. WOB 0-5K, GPM, TD 60 RPM, MOTOR 54 RPM, PP 365 PSI, TORQUE 1500 FT/LBS. DRILL 17 1/2" SURFACE HOLE. DROP GYRO & TOOH TO RUN CASING. Mar MD: 1,450 TVD: 1,450 FOOTAGE: 1,100 MW: 8.9 LB PTD: 17,368 DRILL 17 1/2" HOLE F/ 350' TO 1450'. PROBLEMS W/ CLAY PLUGGING FLOWLINE, POSSUM BELLY, & SHAKERS. R/U & CIRC INSIDE RES. SHOVEL CUTTINGS OUT OF POSSUM BELLY & JET FLOWLINE. RIG UP JET LINE TO POSSUM BELLY FROM TRIP TANK PUMP.;DRILL F/ 350' TO 552'. WOB 5-15K, TD 80 RPM, 500 GPM, MOTOR 80 RPM, PP 500 PSI, TORQUE 3000 FT/LBS. HAD TO STOP DRILLING NUMEROUS TIMES & DIG CLAY OUT OF POSSUM BELLY. CONTROL DRILL DUE TO THE PLUGGING OFF OF FLOWLINE, POSSUM BELLY. DECISION MADE TO CIRC INSIDE RES DUE TO THE PROBLEMS W/ SHAKERS PLUGGING UP.;RIG UP TO CIRC THE INSIDE RES PIT. SAVED AS MUCH SPUD MUD AS POSSIBLE FOR LATER USE.;DRILL F/ 552' TO 1450'. WOB 10-30K, TD RPM, 669 GPM, MOTOR 107 RPM, PP 1200 PSI, TORQUE 3-5K FT/LBS. TD SURFACE 1590'. CIRC & CLEAN HOLE. DROP GYRO & TOOH TO RUN CASING. Mar MD: 1,590 TVD: 1,590 FOOTAGE: 140 MW: 0.0 LB PTD: 17,368 DRILL F/ 1450' TO 1590'. CIRC TO CLEAN HOLE. DROP GYRO. TOOH, L/D 17 1/2" BHA. RUN 13 3/8' CSG & CEMENT. WOC. DRILL F/ 1450' TO 1590'. TD OF 17 1/2" SURFACE HOLE.;CIRC & CONDITION HOLE. PUMPED 3 / 20 BBL SWEEPS. DROP GYRODATA GYRO.;TOOH, RETREIVE GYRO, L/D 2 X 17 3/8" STABS, FLODRIFT TOOL, X/O'S, MUD MOTOR & BIT. STAND 1 STAND 8" DC'S & 4 STANDS 7" DC'S IN DERRICK.;HELD PREJOB SAFETY MEETING W/ PREMIERE CASING CREW.;RIG UP TO RUN CASING.;RUN 37 JTS 13 3/8" 68# J-55 BTC CASING. 2 CENTRALIZERS PER JT ON FIRST 2 JTS THEN ONE CENTRALIZER EVERY THIRD JT TO 339'. 1582'. FLOAT 1535'.;R/D CASING CREW.;CIRC VOLUME OF 6 BPM.;HELD PREJOB SAFETY MEETING W/ TRANS TEX CEMENTERS.;R/U & CEMENT. LEAD: 1135 SKS (384.1 BBLS) TRANS TEX LITE CLASS C + 1% CACL+ 2# GILSONITE # CF, YIELD 1.90, MIX WATER 10.42, 13.0 PPG. TAIL: 325 SKS (96.7 BBLS) TRANS TEX LITE CLASS C + 1% CACL+ 2# GILSONITE # CF, YIELD 1.67, MIX WATER 9.42, 13.9 PPG. CIRCULATED 200 BBLS (591 SKS) TO RESERVE. BUMP PLUG W/ 650 PSI, BLED BACK 1 BBL, FLOATS HELD.;WOC. JET FLOWLINE, DRAIN & WASH OUT CONDUCTOR PIPE, PUMP OUT CELLAR. N/D FLOWLINE. WOC, CUT PIPE & INSTALL WELLHEAD. NIPPLE UP & TEST BOP'S.

3 Mar MD: 1,590 TVD: 1,590 FOOTAGE: MW: 0.0 LB PTD: 17,368 WOC. INSTALL CAMERON WELLHEAD. NIPPLE UP & TEST BOP'S. N/U FLOWLINE INSTALL TURN BUCKLES. WOC.;SLACK OFF CASING, WELDER CUT CONDUCTOR PIPE & 13 3/8'. REMOVE CONDUCTOR & CUT OFF 13 3/8". RECUT & DRESS 13 3/8". CAMERON SERVICE HAND INSTALL & TEST MULTI BOWL WELLHEAD. TEST TO 1000 PSI.;NIPPLE UP BOP'S. INSTALL CONTROL LINES & FUNCTION TEST.;PRESSURE TEST BOP'S & MUD LINES. ANNULAR 250 / 1500 PSI. 5 MIN LOW / 10 MIN HIGH. RAMS, HCR, MANIFOLD & VALVES 250 / 3000 PSI. 5 MIN LOW / 10 MIN HIGH. HIGH PRESS MUD LINES & VALVES PSI FOR 5 MINS. BLIND RAMS & CASING PSI F/ 10 MINS.;N/U FLOWLINE & INSTALL TURN BUCKLES ON BOP'S. SET WEAR BUSHING, P/U BHA & RIH. DRILL OUT CEMENT. DRILL AHEAD 12 1/4" HOLE. Mar MD: 3,000 TVD: 3,000 FOOTAGE: 1,410 MW: 9.8 LB PTD: 17,368 N/U FLOWLINE, SECURE BOP'S. SET WEAR BUSHING. P/U GYRO DATA BHA #1, RIH TO 1531'. DRILL CMT & SHOE. DRILL F/ 1590' TO 3000'. CENTER UP BOP'S & TIGHTEN TURN BUCKLES ON BOP'S.;SET WEAR BUSHING. INSTALL MOUSEHOLE.;P/U GYRO DATA BHA # 1 & SURFACE TEST. RIH, TAG 1533'.;DRILL CEMENT, FLOAT COLLAR, & SHOE F/ 1533' TO 1582'. 1582'. WASH RATHOLE TO 1590'.;DRILL 12 1/4" HOLE F/ 1590' TO 2153'. WOB 15-30K, TD 80 RPM, 670 GPM, MOTOR 107 RPM, PP 1900 PSI, DIFF PSITORQUE 10-15K FT/LBS. CIRC OUTSIDE RESERVE. MW 9.8 PPG. PUMP 30 BBL SWEEP EVERY THIRD STAND. LOST MWD PULSE, UNABLE TO GET SURVEY.;GYRO DATA TROUBLESHOOT MWD. REPROGRAM. GOT IT WORKING!;DRILL 12 1/4" HOLE F/ 2153' TO 3000'. WOB 15-30K, TD 80 RPM, 670 GPM, MOTOR 107 RPM, PP 1900 PSI, DIFF PSI, TORQUE 10-15K FT/LBS. CONTINUE DRILL AHEAD 12 1/4" VERTICAL SECTION. Mar MD: 4,800 TVD: 4,800 FOOTAGE: 1,800 MW: 9.8 LB PTD: 17,368 RIG SUPERVISOR: Jimmy Nobles / David Crow PBTD: DRILL & SURVEY 12 1/4 HOLE F FT. DRILL 12 1/4" HOLE F/ 3000' TO 3941'. WOB 30K, TD 80 RPM, 670 GPM, MOTOR 107 RPM, PP 1900 PSI, DIFF PSI, TORQUE 10-15K FT/LBS. CIRC OUTSIDE RES. MW 9.9 PPG.;RIG SERVICE & DERRICK INSPECTION, REMOVE TRIP NIPPLE & INSTALL ROTATING HEAD RUBBER.;DRILL & SURVEY 12 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=160, GPM=670, DH RPM=107, TD RPM=60-80, TOTAL RPM=190, TDT= , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 12 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=160, GPM=670, DH RPM=107, TD RPM=60-80, TOTAL RPM=190, TDT= , DPP= Mar MD: 6,400 TVD: 6,400 FOOTAGE: 1,600 MW: 9.8 LB PTD: 17,368 DRILL & SURVEY 12 1/4 HOLE F FT. DRILL & SURVEY 12 1/4 HOLE F FT, WOB=10-35K, STK'S=160, GPM=670, DH RPM=107, TD RPM=60-80, TOTAL RPM=190, TDT= , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 12 1/4 HOLE F FT, WOB=10-35K, STK'S=170, GPM=710, DH RPM=115, TD RPM=60-80, TOTAL RPM=195, TDT= , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 12 1/4 HOLE F FT, WOB=10-35K, STK'S=170, GPM=710, DH RPM=115, TD RPM=60-80, TOTAL RPM=195, TDT= , DPP= DRILL TOWARD TD, TD 1ST INTERMEDIATE SECTION, PREP WELL FOR CSG RUN, TOOH, LD BHA. Mar MD: 6,825 TVD: 6,825 FOOTAGE: 425 MW: 9.8 LB PTD: 17,368 DRILL & SURVEY 12 1/4 HOLE F FT, PUMP SWEEP & CIR ON BOTTOM FOR 3 HR'S, SHORT TRIP TO CSG SHOE, TIH, PUMP SWEEP & CIR ON BOTTOM FOR 3 HR'S, TOOH. DRILL & SURVEY 12 1/4 HOLE F FT, WOB=10-40K, STK'S=170, GPM=710, DH RPM=115, TD RPM=60-80, TOTAL RPM=195, TDT= , DPP= ;PULL UP & CIRCULATE WHILE WORKING ON RESERVE PIT PUMP.;DRILL & SURVEY 12 1/4 HOLE F FT, WOB=10-40K, STK'S=170, GPM=710, DH RPM=115, TD RPM=60-80, TOTAL RPM=195, TDT= , DPP= ;DRILL & SURVEY 12 1/4 HOLE F FT, WOB=15K, STK'S=110, GPM=460, DH RPM=75, TD RPM=65, TOTAL RPM=140, TDT= , DPP= "DRILL ON ONE PUMP WHILE REPLACING LINER & SWAB ON #2 PUMP";DRILL & SURVEY 12 1/4 HOLE F FT, WOB=10-40K, STK'S=170, GPM=710, DH RPM=115, TD RPM=60-80, TOTAL RPM=195, TDT= , DPP= "TD (6825FT) THE 1ST INTERMEDIATE SECTION OF THE UNIVERSITY 1-24 UNIT #1H AT ON 3/12/15";PUMP 100 BBL 100 VIS SWEEP, CIRCULATE & ROTATE ON BOTTOM FOR 3 HOURS, PUMP SLUG, MAKE READY TO SHORT TRIP.;SHOR TRIP 56 STANDS TO CSG SHOE (NO DRAG);RIG SERVICE & DERRICK INSPECTION.;TIH (NO TAG OR FILL);PUMP 100 BBL 100 VIS SWEEP, CIRCULATE & ROTATE ON BOTTOM FOR 3 HOURS, PUMP SLUG, MAKE READY TO TOOH.;TOOH. FINISH TOOH, LD BHA #2, RIG UP & RUN 9 5/8 CSG, CEMENT 1ST INTERMEDIATE.

4 Mar MD: 6,825 TVD: 6,825 FOOTAGE: MW: 9.8 LB PTD: 17,368 FINISH TOOH. FINISH TOOH, LD BHA #2, RIG UP CSG CREW, RUN 156 JT'S OF 9 5/8 CSG, LAND CSG ON MANDREL, RIG DOWN CSG CREW, RIG UP CEMENT CREW. "NOTIFY THE TRRC OF UP-COMING CSG RUN & CEMENT JOB AT ON 3/13/15 VIA AUDRY OPERATOR #2";LD BHA #2.;PULL WEAR BUSHING, READY RIG FLOOR TO RUN CSG.;MOVE IN & SPOT / RIG UP CSG CREW, HOLD PJSM WITH SAME.;RUN 156 JOINTS OF 9 5/8, 40#, HCK-55 & J-55, LT&C, 1ST INTERMEDIATE CASING, FLOAT SHOE AT=6807FT, FLOAT JOINT=44.71FT, FLOAT COLLAR AT=6760FT, CASING LANDED ON CAMERON MANDREL & CIRCULATING AT ON 3/14/15. "RUN 63 JOINTS OF HKC-55 & 93 JOINTS OF J-55 FOR A TOTAL OF 156 JOINTS" "1 STANDARD BOW-SPRING CENTRALIZER EVERY 3RD JOINT FROM JOINT FOR A TOTAL OF 52 CENTRALIZERS";RIG DOWN & RELEASE CSG CREW.;MOVE IN & SPOT / RIG UP CEMENT CREW. CEMENT 9 5/8 CSG, PACK OFF MANDREL, PU & MU BHA #3, TIH, DRILL CEMENT & TOOLS, DRILL 8 3/4 HOLE. Mar MD: 6,875 TVD: 6,875 FOOTAGE: 50 MW: 9.8 LB PTD: 17,368 CEMENT 9 5/8 CSG, RIG DOWN CEMENT CREW, PACK OFF & TEST CAMERON MANDREL, RUN TEMP SURVEY, PU & MU BHA #3, TIH WITH BHA #3, DRILL CEMENT & TOOLS, DRILL 8 3/4 HOLE F FT. HOLD PJSM WITH RIG & CEMENT CREW, PSI TEST PUMP & LINES TO 5000 PSI, FOLLOWED BY 20 BBL'S OF FRESH WATER SPACER, START & FINISH 1200 BBL'S OR 2780 SKS OF 11.8#, 2.4 YIELD LEAD CEMENT, START & FINISH 90 BBL'S OR 400 SKS OF 15.6#, 1.8 YIELD TAIL CEMENT, SHUT DOWN & DROP PLUG, DISPLACE 514 BBL'S OF FRESH WATER "LOOSE CIRCULATION 10 BBL'S INTO DISPLACEMENT" BUMP PLUG WITH 1200 PSI, WALK PRESSURE UP TO 1800 PSI, CHECK FLOAT, BLEED BACK 3 BBL'S, PLUG DOWN & HOLDING AT ON 3/14/14. "0 BBL'S OF GOOD CEMENT TO SURFACE" "LEAD CEMENT=2780 SKS WITH 10% GEL, 3% SALT, 2# GILSONTIE, 1/4# CELLOFLAKE, 3% CFL-1" "TAIL CEMENT=400 SKS WITH, 1/4# CELLOFLAKE, 3% CFL-1";RIG DOWN & RELEASE CEMENT CREW.;BACK OUT LANDING JOINT, RUN PACK OFF IN THE HOLE, PACK OFF MANDREL TO 10K, TEST SEAL TO 5K "TEST GOOD" LD PACK OFF TOOLS, INSTALL WEAR-BUSHING, RIG DOWN & RELEASE CAMERON.;READY BHA #3.;MOVE IN & SPOT / RIG UP WIRELINE TRUCK.;RIH WITH APOLLO TEMPERATURE SURVEY TOOL. "TOP OF LEAD CEMENT AT 4330FT" "TOP OF TAIL CEMENT AT 6680FT" ROOH, LD TOOLS, RIG DOWN & RELEASE APOLLO.;PU, MU, SCRIBE, ORIENTATE & SURFACE TEST BHA #3.;TIH WITH BHA #3, STOP AT 6700FT.;RIG SERVICE, INSTALL ROTATING HEAD RUBBER, PSI TEST CSG TO 1500 PSI FOR 10 MIN "TEST GOOD" TAG UP AT 6730FT, MAKE READY TO DRILL CEMENT.;DRILL CEMENT & TOOLS F FT.;DRILL & SURVEY 8 3/4 F FT, WOB=10-35K, STK'S=100, GPM=420, DH RPM=108, TD RPM=60-80, TOTAL RPM=188, TDT= , DPP= Mar MD: 8,400 TVD: 8,400 FOOTAGE: 1,525 MW: 9.8 LB PTD: 17,368 DRILL & SURVEY 8 3/4 HOLE F FT. DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= DRILL TOWARD KOP. Mar MD: 9,625 TVD: 9,625 FOOTAGE: 1,225 MW: 9.8 LB PTD: 17,368 DRILL & SURVEY 8 3/4 F FT. DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= DRILL TOWARD KOP. Mar MD: 9,925 TVD: 9,925 FOOTAGE: 300 MW: 9.8 LB PTD: 17,368 DRILL & SURVEY 8 3/4 HOLE F FT, PUMP SWEEP & CIR BOTTOMS UP, TOOH, LD BHA #3, PU & MU BHA #4. DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= ;PUMP 50 BBL 100 VIS SWEEP & CIRCULATE BOTTOMS, PUMP SLUG, MAKE READY TO TOOH.;TOOH.;LD BHA #3 "BIT, MUD MOTOR, STABILIZER, UBHO SUB & MONEL PACKED OFF WITH FINE CUTTINGS" CLEAN OUT TOOLS, PU, MU, SCRIBE, ORIENTATE & SURFACE TEST BHA #4.;TIH WITH BHA #4. FINISH TIH, DRILL TOWARD KOP.

5 Mar MD: 10,355 TVD: FOOTAGE: 430 MW: 9.8 LB PTD: 17,368 FINISH TIH, DRILL & SURVEY 8 3/4 HOLE F FT, PUMP SWEEP & CIR BOTTOMS UP, TOOH, LD BHA #4, PU & MU BHA #5. TIH.;STOP AT CSG SHOE, REMOVE TRIP NIPPLE, INSTALL ROTATING HEAD RUBBER.;FINISH TIH.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=130, TD RPM=60-80, TOTAL RPM= , TD , DPP= "REACH KOP (10355FT) AT ON 3/18/14";PUMP 100 BBL 100 VIS SWEEP & CIRCULATE BOTTOMS UP, PUMP SLUG, MAKE READY TO TOOH.;TOOH.;LD 7 INCH DC'S & BHA #4.;PU, MU, SCRIBE, ORIENTATE & SURFACE TEST BHA #5. FINISH MU CURVE BHA, TIH, BEGIN DRILLING 8 3/4 CURVE. Mar MD: 10,355 TVD: FOOTAGE: MW: 9.8 LB PTD: 17,368 TIH WITH CURVE BHA, HAVE TROUBLES WITH TOTCO, DIR TOOLS & TOP DRIVE, REPAIR PROBLEMS WHILE WORKING PIPE. TIH WITH BHA #5.;STOP AT CSG SHOE, PULL TRIP NIPPLE & INSTALL ROTATING HEAD RUBBER, BREAK CIRCULATION & TEST DIRECTIONAL TOOLS.;CONTINUE TIH.;STOP AT 9000FT, ATTEMPT TO TEST DIRECTIONAL TOOLS, STRING PRESSURED UP, BEGIN HAVING TOTCO PROBLEMS AT THE SAME TIME, BLEED OFF PRESSURE.;TOOH TO CSG SHOE, TOTCO ON LOCATION WORKING ON SYSTEM, BREAK CIRCULATION & TEST DIRECTIONAL TOOLS.;TIH TO 9000FT.;SCREW INTO STRING & BREAK CIRCULATION, DIRECTIONAL TOOLS WORKING, UNSCREW FROM TOP DRIVE & LOOSE HYD CONTROL, ABLE TO WORK PIPE UP & DOWN ONLY, NO OTHER TOP DRIVE FUNCTION WORKING, FIND 19 PIN CONNECTOR BURNT, CALL & WAIT ON TECH & NEW PARTS, CHANGE OUT 19 PIN CONNECTOR, TOP DRIVE STILL NOT WORKING, CONTINUE WORKING PIPE & DIAGNOSING TOP DRIVE TROUBLES. FIX TOP DRIVE, BREAK CIRCULATION, TEST TOOLS, TIH, DRILL 8 3/4 CURVE. Mar MD: 10,355 TVD: FOOTAGE: MW: 9.8 LB PTD: 17,368 FINISH TOP DRIVE REPAIR, TOOH TO CSG SHOE, ATTEMPT TO BREAK CIR WITHOUT SUCCESS, TOOH, LD BHA #5, CLEAN OUT MANIFOLDS, CIR SYSTEM CLEAN, PU & MU BHA #6, TIH WITH BHA #6, WASH & REAM, CONTINUE TIH. FINISH REPAIR ON TOP DRIVE, FUNCTION TEST TOP DRIVE "ALL SYSTEMS WORKING" TO DATE (1) ENCODER & (1) ENCODER CABLE CHANGED OUT LAST WELL, (3) AC PIGTAILS, (1) 42 PIN PIGTAIL, (1) AC SERVICE LOOP CHANGED ON RIG MOVE, (1) 19 PIN PIGTAIL & (1) 19 PIN SERVICE LOOP CHANGED OVER THE LAST DAY. ALL ELECTRIC CABLES NOW HAVE BEEN CHANGED ON TOP DRIVE.;TOOH TO CSG SHOE.;ATTEMPT TO BREAK CIRCULATION, STRING PRESSURING UP, ROTATE & SURGE OFF PRESSURE'S FOR 1 HOUR WITHOUT SUCCESS, MAKE READY TO TOOH. "TOP DRIVE & TOTCO SYSTEMS WORKING WITHOUT PROBLEMS";TOOH. "RECEIVE (550) JT'S OF 4 INCH FH DP, (30) JT'S 4 INCH FH HWDP & TOOLS FROM IRONGATE 3/20/15";INSPECT & LAYDOWN BHA #5, FIND TOOLS PACKED WITH CUTTINGS FROM UBHO SUB TO TOP OF MUD MOTOR.;CLEAN OUT ACTIVE SYSTEM SUCTION MANIFOLDS, MUD PUMP SUCTIONS, DRAIN STANDPIPE & KELLY HOSE, RUN 1 STAND OF DP IN HOLE CIRCULATE ACROSS SHAKERS AT 500 GPM FOR 1 HOUR.;PU, MU, SCRIBE, ORIENTATE & SURFACE TEST BHA #6.;TIH WITH BHA #6.;STOP AT CSG SHOE, PULL TRIP NIPPLE, INSTALL ROTATING HEAD RUBBER, BREAK CIRCULATION & TEST DIRECTIONAL TOOLS.;TIH.;TAG UP AT 8755FT, WASH & REAM F FT.;CONTINUE TIH. FINISH TIH, BEGIN DRILLING 8 3/4 CURVE. Mar MD: 10,860 TVD: 10,731 FOOTAGE: 505 MW: 9.8 LB PTD: 17,368 FINISH TIH, PRECAUTIONARY WASH & REAM F FT, DRILL & SURVEY 8 3/4 HOLE F FT. FINISH TIH.;PRECAUTIONARY WASH & REAM F FT.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-25K, STK'S=120, GPM=500, DH RPM=120, TD RPM=0-30, TOTAL RPM= , TD , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-25K, STK'S=120, GPM=500, DH RPM=120, TD RPM=0-30, TOTAL RPM= , TD , DPP= DRILL TOWARD LANDING POINT. Mar MD: 11,300 TVD: FOOTAGE: 440 MW: 9.8 LB PTD: 17,368 DRILL & SURVEY 8 3/4 HOLE F FT, WORK TIGHT HOLE, DRILL & SURVEY 8 3/4 HOLE F FT. DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-25K, STK'S=120, GPM=500, DH RPM=120, TD RPM=0-30, TOTAL RPM= , TD , DPP= ;WORK TIGHT HOLE F FT.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-25K, STK'S=120, GPM=500, DH RPM=120, TD RPM=0-30, TOTAL RPM= , TD , DPP= ;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-25K, STK'S=120, GPM=500, DH RPM=120, TD RPM=0-30, TOTAL RPM= , TD , DPP=

6 Mar MD: 11,439 TVD: 11,085 FOOTAGE: 139 MW: 9.8 LB PTD: 17,368 DRILL & SURVEY 8 3/4 HOLE F FT, WORK TIGHT HOLE, PUMP SWEEP & CIR 3 HR'S, SHORT TRIP, WASH & REAM, PUMP SWEEP & CIR 4 HR'S. DRILL & SURVEY 8 3/4 WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=120, GPM=500, DH RPM=120, TD RPM=0-30, TOTAL RPM= , TD , DPP= "NOTIFY THE TRRC OF UPCOMING TD, CASING RUN & CEMENT JOB AT ON 3/23/15 VIA LUCY" "11390FT=95% LIMESTONE, 5% SHALE, TRACE CHERT" "11420FT=100% LIMESTONE, TRACE CHERT";WORK TIGHT HOLE F FT.;PUMP 100 BBL 100 VIS SWEEP, CIRCULATE & ROTATE ON BOTTOM FOR 3 HOURS.;SHORT TRIP 85 STANDS "NO DRAG" TIH WITH SAME, TAG UP AT 8700FT;WASH & REAM F FT.;FINISH TIH.;PRECAUTIONARY WASH & REAM F FT.;PUMP 50 BBL 100 VIS SWEEP "1ST SWEEP BROUGHT UP PEA SIZED GRAVEL" PUMP 2ND 50 BBL 100 VIS SWEEP "2ND SWEEP BROUGHT UP PEA SIZED GRAVEL & SMALLER" CIRCULATE & ROTATE ON BOTTOM FOR 4 HOURS. MAKE 2ND SHORT TRIP, TOOH, MAKE READY TO RUN CSG. Mar MD: 11,439 TVD: 11,085 FOOTAGE: MW: 9.6 LB PTD: 17,368 RIG SUPERVISOR: David Crow / Jimmy Nobles PBTD: CIRC SWEEP, SHORT TRIP, WASH & REAM F FT, PUMP SWEEP & CIRC, SPOT PILL, TOOH TO SHOE. SLIP & CUT DRILL LINE, TOOH, L/D HWDP & BHA. R/U & RUN CSG. FINISH CIRCULATING SWEEP "3RD SWEEP BROUGHT UP FINE TO NO CUTTINGS";SHORT TRIP 15 STANDS "NO DRAG" TIH WITH SAME "NO TAG";PRECUATIONARY WASH & REAM F FT.;PUMP 100 BBL 100 VIS SWEEP, CIRCULATE & ROTATE ON BOTTOM FOR 2 HOUR'S, TAKE SURVEY, SPOT 100 BBL'S OF 12#, 2% BEADS, 100 VIS MUD ON BOTTOM, MAKE READY TO TOOH.;TOOH, STOP AT CSG SHOE.;SLIP & CUT DRILL LINE. REMOVE R/H & INSTALL TRIP NIPPLE.;FINISH TOOH. L/D HWDP & DIR BHA. BIT IN BAD SHAPE.;RETRIEVE WEAR BUSHING.;CLEAR FLOOR & PREP TO RUN CSG.;HELD PREJOB SAFETY MEETING W/ PREMIERE CASING CREW.;R/U PREMIERE TOOLS & CRT.;RUNNING 2ND INTERMEDIATE 7" 26# P-110 LTC CSG. RUN 7" 26# CSG & CEMENT. Mar MD: 11,439 TVD: 11,085 FOOTAGE: MW: 9.6 LB PTD: 17,368 RUN 259 JTS 7" CASING. TIGHT HOLE F/ 11,096' TO 11,250'. PUMP FW PRIOR TO CEMENTING. RUN 7" 26# P-110 LTC CASING.;PREMIERE WORK ON CRT TOOL, DIES NOT RELEASING & HANGING ON COLLAR.;RUN 7" 26# P-110 LTC CASING. BREAK SHOE, ONLY GETTING PARTIAL RETURNS. TAG 11,096'.;WORK TIGHT HOLE & 3 BPM, HOLE PACKING OFF. NO RETURNS. START PUMPING FRESH WATER. WORK PIPE DOWN TO WITHIN 2 FT FROM LANDING, CRT TOOL HITTING ROTARY BEFORE HANGER LANDED OUT IN WELLHEAD. TIGHT HOLE F/ 11,096' TO 11,250'. LAST 4 JTS WENT DOWN GOOD.;RIG DOWN PREMIERE CRT TOOL & R/U BALES & SIDE DOOR ELEVATORS. LAND CASING HANGER IN WELLHEAD. RAN 259 JTS 7" 26# P-110 LTC CASING. RAN CENTRALIZER EVERY 3RD JOINT F/ 8014' TO 5519'. 11,410'. FLOAT 11,359'.;PUMP FRESH WATER PRIOR TO CEMENTING. NO RETURNS UNTIL FW ROUNDED THE SHOE THEN STARTED GETTING SOME PARTIAL RETURNS BACK. HOLD SAFETY MEETING W/ CEMENTERS. CEMENT 7" CASING, SET PACKOFF ON HANGER & TEST. TEST BOP'S. LAY DOWN 5" DRILL PIPE. Mar MD: 11,439 TVD: 11,085 FOOTAGE: MW: 9.0 LB PTD: 17,368 CEMENT 7" CSG, BACK OUT LANDING JT, SET PACKOFF, TEST BOP'S, LAY DN 5" DP. FINISH R/U TRANS TEX CEMENTERS & PRESSURE TEST LINES TO 4000 PSI.;PUMP 20 BBLS FW AHEAD, MIX 700 SKS (301 BBLS) LEAD 11.8 PPG, 2.42 YIELD, GAL/SK MIX WATER, 10% GEL, 3% SALT,.2# GILS, 1/4 # CF,.4% CFL-1,.3% CR-1, 2% CFR-1,.05% CAS-1. PUMP 400 SKS (93 BBLS) TAIL 14.4 PPG, 1.31 YIELD, 5.59 GAL/SK MIX WATER, 2% GEL, 3% SALT, 1/4# CF,.4% CFL-1,.35% CR-1,.2% CFR-1. DROP PLUG & DISPLACE W/ 434 BBLS FW, BUMP PLUG W/ 3000 PSI, BLED BACK 3 BBLS, FLOATS HOLDING. HAD GOOD RETURNS THROUGH MOST OF CEMENT JOB, DN TO PARTIAL RETURNS AT THE END OF JOB. FINAL LIFT PRESS 2500 PSI.;R/D & RELEASE TRANS TEX CEMENTERS.;BACK OUT LANDING JT. CAMERON RUN & SET PACKOFF & BIT GUIDE.;TEST PACKOFF, BOP'S, CHOKE MANIFOLD, & HP MUD LINES. RAMS, PACKOFF, & VALVES 250 / 3000 PSI F/ 10 MINS. ANNULAR 250 / 1500 PSI F/ 10 MINS. HIGH PRESSURE MUD LINES 4000 PSI F/ 10 MINS.;CLEAN UP FLOOR & PREP TO LAY DOWN 5" DRILL PIPE.;LAY DOWN 5" DRILL PIPE F/ MOUSEHOLE.;WORK ON IRON ROUGHNECK.;LAY DOWN 5" DRILL PIPE F/ MOUSEHOLE. FINISH LAY DOWN 5" DP, P/U DIR BHA & RIH PICKING UP 4" DP. Mar MD: 11,439 TVD: 11,085 FOOTAGE: MW: 9.0 LB PTD: 17,368 FINISH L/D 5" DP. R/U FLOOR F/ 4" TUBULARS. P/U BHA # 7 & RIH, P/U 4" DP F/ RACKS. FINISH L/D 5" DRILL PIPE F/ MOUSEHOLE.;CLEAR ALL 5" HANDLING TOOLS OFF FLOOR & RIG UP TO HANDLE 4" TUBULARS. CHANGE OUT SAVER SUB. RECOVER OLD & INSTALL NEW CORROSION RING. LOAD PIPE RACK WITH 4" DP & STRAP.;SERVICE RIG.;P/U GYRO DATA BHA # 7. SCRIBE & SURFACE TEST.;RIH PICKING UP 4" DRILL PIPE.;WORK ON IRON ROUGHNECK.;CONTINUE RIH PICKING UP 4" DP F/ RACKS. BIT DEPTH REPORT TIME. FINISH P/U 4" DP, DRILL OUT CEMENT. DRILL & LAND 6 1/4" CURVE.

7 Mar MD: 11,750 TVD: 11,119 FOOTAGE: 311 MW: 9.1 LB PTD: 17,368 FINISH P/U 4" DP. DRILL OUT CEMENT. DRILL 6 1/4" CURVE F/ 11,439' TO 11,750'. RIH PICKING UP 4" DP. 11,175'.;PULL TRIP NIPPLE & INSTALL R/H RUBBER.;DRILL OUT CEMENT, PLUG, FLOAT COLLAR, & SHOE. WASH & REAM RATHOLE. FOUND FLOAT COLLAR, SHOE & BOTTOM 20' HIGH. DOUBLE CHECKED PIPE COUNT ON LOCATION & IT IS CORRECT. WILL STRAP OUT ON NEXT TRIP TO CONFIRM TALLY.;DRILL (SLIDE & ROTATE) 6 1/4" CURVE F/ 11,439' TO 11,750. WOB 18-23K, TD 40 RPM, MOTOR 145 RPM, PP 1400 PSI, DIFF PSI, TORQUE 5K. MW 9.1 PPG. NOTE: HADCO ON LOCATION START INSPECTING 5" DP & BHA. DRILL 6 1/4" LATERAL. POSSIBLY TRIP F/ LATERAL BHA. Mar MD: 12,380 TVD: 11,100 FOOTAGE: 630 MW: 9.1 LB PTD: 17,368 DRILL 6 1/4" LATERAL F/ 11,750' TO 12,380'. DRILL 6 1/4" LATERAL (SLIDE & ROTATE) F/ 11,750' TO 11,857'. WOB 18-23K, TD 45 RPM, MOTOR 145 RPM, PP 1450 PSI, DIFF PSI, TORQUE 5K. MW 9.1 PPG.;SERVICE RIG & TAKE SLOW PUMP RATES.;DRILL 6 1/4" LATERAL (SLIDE & ROTATE) F/ 11,857' TO 12,263'. WOB 18-21K, TD 60 RPM, MOTOR 145 RPM, PP 1450 PSI, DIFF PSI, TORQUE 7K. MW 9.1 PPG.;SERVICE RIG.;DRILL 6 1/4" LATERAL (SLIDE & ROTATE) F/ 12,263' TO 12,380'. WOB 18-21K, TD 60 RPM, MOTOR 145 RPM, PP 1450 PSI, DIFF PSI, TORQUE 7K. MW 9.1 PPG. CONTINUE DRILLING 6 1/4" LATERAL. Mar MD: 12,808 TVD: 11,086 FOOTAGE: 428 MW: 9.1 LB PTD: 17,368 DRILL 6 1/4" LATERAL F/ 12,380' TO 12,808'. TOOH TO CHANGE BIT & BHA. DRILL 6 1/4" LATERAL (SLIDE & ROTATE) F/ 12,380' TO 12,524'. WOB 18-25K, TD 60 RPM, GPM 250, MOTOR 145 RPM, PP 1450 PSI, DIFF PSI, TORQUE 7K. MW 9.1 PPG.;SERVICE RIG & TAKE SLOW PUMP RATES.;DRILL 6 1/4" LATERAL (SLIDE & ROTATE) F/ 12,524' TO 12,808'. WOB 18-25K, TD 60 RPM, GPM 275, MOTOR 160 RPM, PP 1650 PSI, DIFF PSI, TORQUE 8-9K.;TOOH TO SHOE.;REMOVE R/H & INSTALL TRIP NIPPLE.;TOOH TO CHANGE BIT & BHA. STRAP PIPE. FINISH TOOH, CHANGE BHA, RIH & CONTINUE DRILL 6 1/4" LATERAL. Apr MD: 13,125 TVD: 11,075 FOOTAGE: 317 MW: 9.1 LB PTD: 17,368 FINISH TOOH, P/U NEW BHA, RIH W/ BHA # 8. DRILL 6 1/4" LATERAL F/ 12,808' TO 13,125'. TOOH, L/D DIR BHA #7. BIT IN PRETTY GOOD SHAPE.;P/U GYRO DATA 5" MOTOR & LATERAL BHA. SCRIBE & SURFACE TEST.;SERVICE RIG.;RIH W/ GYRO DATA BHA # 8. FILL EVERY 30 STANDS TO 11,000'.;REMOVE TRIP NIPPLE & INSTALL R/H.;FINISH RIH TO 12,775'. WASH DOWN F/ 12,775' TO 12,808'.;DRILL 6 1/4" LATERAL F/ 12,808' TO 13,125'. WOB 20-28K, 275 GPM, TD RPM, MOTOR 217 RPM, PP 1650 PSI, DIFF PSI, TORQUE 8-14K FT/LBS. 95% LS & 5% 100% LS W/ TRACE OF 13,060'. CONTINUE DRILLING 6 1/4" LATERAL. Apr MD: 13,276 TVD: 11,073 FOOTAGE: 151 MW: 9.1 LB PTD: 17,368 TRIP F/ NEW BIT & MOTOR. DRILL 6 1/4" LATERAL F/ 13,125' TO 13,276'. DRILL 6 1/4" LATERAL F/ 13,125' TO 13,193'. WOB 20-28K, 275 GPM, TD RPM, MOTOR 239 RPM, PP 1700 PSI, DIFF PSI, TORQUE 8-14K FT/LBS. ROP FALLING OFF & NUMEROUS MOTOR STALLS.;TOOH F/ BIT & MOTOR CHANGE. PULL R/H & INSTALL TRIP SHOE. L/D MOTOR.;P/U GYRO DATA BHA #9, SURFACE TEST.;RIH W/ BHA #9 TO SHOE. FILL EVERY 30 STDS. INSTALL SHOE.;DRILL 6 1/4" LATERAL F/ 13,193' TO 13,276'. WOB 18-20K, 285 GPM, TD 70 RPM, MOTOR 75 RPM, PP 1700 PSI, DIFF PSI, TORQUE 7,000 FT/LBS. CONTINUE DRILLING 6 1/4" LATERAL. Apr MD: 13,900 TVD: 11,050 FOOTAGE: 624 MW: 9.1 LB PTD: 17,368 DRILL 6 1/4" LATERAL F/ 13,276' TO 13,900'. DRILL 6 1/4" LATERAL F/ 13,276' TO 13,561'. WOB 20-25K, 285 GPM, TD RPM, MOTOR 74 RPM, PP 1800 PSI, DIFF PSI, TORQUE 7,000 FT/LBS.;SERVICE RIG & TAKE SLOW PUMPS RATES.;DRILL 6 1/4" LATERAL F/ 13,561' TO 13,847'. WOB 19-25K, 285 GPM, TD RPM, MOTOR 74 RPM, PP 1800 PSI, DIFF PSI, TORQUE 7,000 FT/LBS.;SERVICE RIG.;DRILL 6 1/4" LATERAL F/ 13,847' TO 13,900'. WOB 19-25K, 285 GPM, TD 70 RPM, MOTOR 74 RPM, PP 1800 PSI, DIFF PSI, TORQUE 7,500 FT/LBS. BUILDING IN ROTATION. CONTINUE DRILLING 6 1/4" LATERAL.

8 Apr MD: 14,400 TVD: 11,045 FOOTAGE: 500 MW: 9.1 LB PTD: 17,368 RIG SUPERVISOR: Jimmy Nobles / David Crow PBTD: DRILL 6 1/4" LATERAL F13,900-14,400FT. DRILL 6 1/4" LATERAL F/ 13,900' TO 14110'. WOB 19-25K, 285 GPM, TD 70 RPM, MOTOR 74 RPM, PP 1800 PSI, DIFF PSI, TORQUE 6-8K FT/LBS. BUILDING IN ROTATION & WALKING RIGHT. 100% LIMESTONE, TRACE CHERT AT 13970FT. 100% LIMESTONE, TRACE CHERT AT 14150FT. 100% LIMESTONE AT 14270FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-30K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= ;RIG SERVICE.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-30K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, 5% CHERT AT 14360FT. CONTINUE DRILLING 6 1/4" LATERAL. Apr MD: 14,605 TVD: 11,050 FOOTAGE: 205 MW: 9.1 LB PTD: 17,368 DRILL & SURVEY 6 1/4 HOLE F FT, CIR BOTTOMS UP, TOOH, LD BHA #9, PU & MU BHA #10, TIH WITH BHA #10. DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-30K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 14420FT. 100% LIMESTONE, TRACE CHERT AT 14540FT. 100% LIMESTONE AT 14605FT.;CIRCULATE BOTTOMS UP, PUMP SLUG, MAKE READY TO TOOH.;TOOH.;LD BHA #9, PU, MU, SCRIBE, ORIENTATE & SURFACE TEST BHA #10.;RIG SERVICE & DERRICK INSPECTION.;TIH WITH BHA #10. TIH, STOP AT CSG SHOE SLIP & CUT DRILL LINE, FINISH TIH, DRILL AHEAD. Apr MD: 15,050 TVD: 11,046 FOOTAGE: 445 MW: 9.2 LB PTD: 17,368 TIH WITH BHA #10, SLIP & CUT DRILL LINE, FINISH TIH, DRILL & SURVEY 6 1/4 HOLE F FT. TIH WITH BHA #10.;STOP AT 7800FT, FLOAT LEAKING, KELLY UP ON STRING, PUMP & WORK STRING ATTEMPTING TO CLOSE FLOAT, FLOAT NOT HOLDING, INSTALL 2ND FLOAT OF TOP OF HWDP.;CONTINUE TIH.;STOP AT CSG SHOE, SLIP & CUT 60FT OF 1 3/8 DRILLING LINE.;FINISH TIH.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-25K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE AT 14605FT. 100% LIMESTONE, TRACE CHERT AT 14750FT. 100% LIMESTONE, TRACE CHERT AT 14840FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-25K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE AT 14900FT. 100% LIMESTONE, TRACE CHERT AT 14990FT. Apr MD: 15,700 TVD: 11,026 FOOTAGE: 650 MW: 9.2 LB PTD: 17,368 DRILL & SURVEY 6 1/4 HOLE F FT. DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 15020FT. 100% LIMESTONE, TRACE CHERT AT 15140FT. 100% LIMESTONE, TRACE CHERT AT 15260FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE AT 15390FT. 100% LIMESTONE, TRACE CHERT AT 15440FT. 100% LIMESTONE, TRACE CHERT AT 15590FT. 100% LIMESTONE, TRACE CHERT AT 15650FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP=

9 Apr MD: 16,180 TVD: 11,014 FOOTAGE: 480 MW: 9.2 LB PTD: 17,368 DRILL & SURVEY 6 1/4 HOLE F FT. DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 15710FT. 100% LIMESTONE, TRACE CHERT AT 15800FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 15860FT. 100% LIMESTONE, TRACE CHERT AT 15950FT. 95% LIMESTONE, 5% CHERT AT 16070FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, 5% CHERT AT 16100FT. 100% LIMESTONE, TRACE CHERT AT 16160FT. Apr MD: 16,525 TVD: 11,019 FOOTAGE: 345 MW: 9.2 LB PTD: 17,368 DRILL & SURVEY 6 1/4 HOLE F FT, CIR ON BOTTOM FOR 1 HR, PUMP SLUG, TOOH. DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 16190FT. 100% LIMESTONE, TRACE CHERT AT 16280FT. 95% LIMESTONE, 5% CHERT AT 16345FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 16370FT. 95% LIMESTONE, 5% CHERT AT 16400FT. 95% LIMESTONE, 5% CHERT AT 16490FT. 70% LIMESTONE, 30% CHERT AT 16525FT.;CIRCULATE & ROTATE ON BOTTOM FOR 1 HOUR, PUMP SLUG, MAKE READY TO TOOH.;TOOH. FINISH TOOH, LD BHA #10, PU & MU BHA #11, TIH, RESUME DRILLING AHEAD. Apr MD: 16,700 TVD: 11,020 FOOTAGE: 175 MW: 9.2 LB PTD: 17,368 TOOH, LD BHA #10, PU & MU BHA #11, TIH WITH BHA #11, BREAK CIR & TAKE SURVEY, DRILL & SURVEY 6 1/4 HOLE F FT. TOOH.;LD BHA #10, BIT IN GOOD SHAPE, PU, MU, SCRIBE, ORIENTATE & SURFACE TEST BHA #11.;TIH WITH BHA #11, STOP AT 2000FT.;RIG SERVICE & DERRICK INSPECTION.;PU, MU & TEST NOV AGITATOR.;TIH WITH BHA #11.;KELLY UP & BREAK CIRCULATION, TAKE SURVEY, MAKE READY TO DRILL AHEAD.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, 5% CHERT AT 16540FT. 100% LIMESTONE, TRACE CHERT AT 16640FT. Apr MD: 17,096 TVD: 10,999 FOOTAGE: 396 MW: 9.2 LB PTD: 17,368 DRILL & SURVEY 6 1/4 HOLE F FT, REACH TD (17096FT) PUMP SWEEP & CIR 6 HR'S, SHORT TRIP 20 STANDS. DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 16700FT. 95% LIMESTONE, 5% CHERT AT 16790FT. 95% LIMESTONE, 5% CHERT AT 16850FT. 100% LIMESTONE, TRACE CHERT AT 17000FT.;RIG SERVICE & DERRICK INSPECTION.;DRILL & SURVEY 6 1/4 HOLE WHILE SLIDING & ROTATING F FT, WOB=10-35K, STK'S=69, GPM=290, DH RPM=75, TD RPM=0-70, TOTAL RPM=0-145, TD , DPP= % LIMESTONE, TRACE CHERT AT 17030FT. 70% LIMESTONE 30% CHERT AT 17050FT. 100% LIMESTONE AT 17096FT. TD (17096FT) THE PRODUCTION SECTION OF THE UNIVERSITY 1-24 #1H AT ON 4/10/15.;PUMP 50 BBL 100 VIS SWEEP, CIRCULATE & ROTATE ON BOTTOM FOR 6 HOURS.;SHORT TRIP 20 STANDS "NO DRAG" TIH WITH SAME "NO TAG / FILL" CIR 6 HR'S, TOOH, LD DIR TOOLS, RIG UP & RUN 4.5 PROD LINER WITH NCS SLEEVES.

10 Apr MD: 17,096 TVD: 10,999 FOOTAGE: MW: 9.2 LB PTD: 17,368 CIR 6 HR'S, TOOH, LD DIR TOOLS, RIG UP CSG CREW, RUN 4.5 LINER WITH NCS SLEEVES. PUMP 50 BBL 100 VIS SWEEP, CIRCULATE & ROTATE ON BOTTOM FOR 6 HOUR'S, PUMP SLUG, MAKE READY TO TOOH. "RELEASE DIVERSIFIED MUD LOGGERS AT ON 4/11/15";TOOH.;LAY DOWN DIRECTIONAL TOOLS. "RELEASE GYRO DATA AT ON 4/11/15";MOVE IN & SPOT / RIG UP CASING CREW, HOLD PJSM WITH RIG, NCS TOOL HANDS, WEATHERFORD TOOL HAND & CASING CREW'S. DURING SAFETY MEETING TONG TRUCK DIED & WOULD NOT RE-START.;WAIT ON 2ND TONG TRUCK FROM TOWN.;RUN 146 JOINT'S OF 4 1/2, 11.6#, P-110, BPN PRODUCTION CASING, FLOAT SHOE AT 17094FT, FLOAT JOINT=43.50FT, FLOAT COLLAR AT 17046FT, LANDING COLLAR AT 17044FT, NCS SLEEVES EVERY 4TH JOINT FROM JOINT FOR A TOTAL OF 30 SLEEVES. "SEE ATTACHED PIPE TALLY FOR EXACT SLEEVE PLACEMENT" FINISH MU LINER & SLEEVES, RIG DOWN CSG CREW, RUN LINER WITH DP, SET HANGER, CEMENT PROD LINER. Apr MD: 17,096 TVD: 10,999 FOOTAGE: MW: 9.2 LB PTD: 17,368 FINISH RUNNING LINER, PU & MU HANGER, TIH WITH LINER & DP, LINER & TOOLS ON BOTTOM / IN PLACE, CIR ON BOTTOM FOR 1 HR, ATTEMPT TO SET HANGER, CEMENT PROD LINER, DISPLACE ANNULAR, TOOH, LD SETTING TOOL FINISH RUNNING LINER, PU & MU WEATHERFORD LINER HANGER.;CIRCULATE WHILE RIGGING DOWN CASING CREW.;TIH WITH LINER & 4 INCH DP.;STOP AT 7 INCH CSG SHOE & CIRCULATE BOTTOMS UP.;TIH WITH LINER & 4 INCH DP, LINER ON BOTTOM & CIRCULATING AT ON 4/12/15.;CIRCULATE ON BOTTOM FOR 1 HOUR.;MAKE READY TO SET HANGER, DROP 1.5 INCH BALL & WAIT 20 MIN, WALK RATE UP TO 4 BPM, LAND BALL WITH 4200 PSI, SEE BALL SEAT SHEAR, BEGIN WORKING TORQUE DOWN TO RELEASE FROM HANGER, AFTER 4 HOURS & STILL UNABLE TO SEE PROPER SIGNS OF BEING RELEASED FROM HANGER TALK WITH WEATHERFORD & ELEVATION ON OPTIONS, MAKE DECISION TO CEMENT.;MOVE IN & SPOT / RIG UP CEMENT CREW, HOLD PJSM WITH SAME.;PSI TEST PUMP & LINES TO 5000 PSI, FOLLOWED BY 20 BBL'S OF FRESH WATER SPACER, START & FINISH 180 BBL'S OR 585 SKS OF 13.2 #, 1.25 YIELD LEAD CEMENT, SHUT DOWN & DROP PLUG, WASH UP PUMP & LINES TO RESERVE PIT, BEGIN 216 BBL 2% KCL DISPLACEMENT, AT 320 BBL'S TOTAL PUMPED SEE CEMENT AT RESERVE PIT, MAKE DECISION TO CIRCULATE OUT CEMENT, PUMP 375 BBL'S OF FRESH WATER, WITH ANNULAR "10239FT-SURFACE" FULL OF FRESH WATER LAYDOWN SINGLE & CEMENT HEAD, MAKE READY TO TOOH.;TOOH, LD SETTING TOOL, RETURN SETTING TOOL TO WEATHERFORD FOR RE-DRESS, SHUT IN WELL & WAIT ON ORDERS. WAIT ON ORDERS. Apr MD: 17,096 TVD: 10,999 FOOTAGE: MW: 9.2 LB PTD: 17,368 WAIT ON ORDERS, TIH WITH SLICK SECONDARY PACKOFF, WASH INTO LINER, ESTABLISH RATE & BEGIN PUMPING, LAND PLUG, LD DP. WAIT ON ORDERS.;WEATHERFORD TOOLS ON LOCATION AT ON 4/13/15, PU & MU SECONDARY PACKOFF, MAKE READY TO TIH WITH SAME.;TIH WITH SECONDARY PACKOFF.;TAG UP AT,10127FT, WORK UP & DOWN RE-TAGGING AT THE SAME SPOT, PULL UP & BEGIN PUMPING AT 3 BPM, WASH DOWN INTO LINER FROM FT "FELT LIKE WE WERE PUSHING DART / PLUG INTO TOP OF LINER" BEGIN PUMPING DOWN LINER WITH FULL RETURNS, AFTER 1 HOUR OF PUMPING LINER MOVED DOWN TO 10140FT, CONTINUE PUMPING DOWN LINER ATTEMPTING TO LAND THE PLUG, AFTER PUMPING "3 BPM 3600 PSI" 2 CASING VOLUMES OR 224 BBL'S DECIDE PLUG IS LANDED BUT DAMAGED IN SOMEWAY & NOT COMPLETLEY HOLDING, KICK OUT PUMP PRESURE BLEED OFF TO 1200 PSI, ZERO STROKE COUNTER & BEGIN PUMPING "3 BPM PSI" AFTER 10 MIN RAISE PUMP RATE TO 4 BPM & 3900 PSI, CONTINUE PUMPING 4 BPM FOR 120 BBL'S, SEE PRESSURE FALL OFF 100 PSI, MAKE DECISION TO CALL ELLISON FLUID CALIPER TO ENSURE WE ARE PUMPING OUT THE END OF LINER, CONTINUE PUMPING 4 BPM WHILE WAITING ON ELLISON TO ARRIVE, ELLISON ON LOCATION AT ON 4/13/15, AT 500 BBL'S PUMPED BEGIN SEEING MUD RETURNS, CONTINUE PUMPING TRYING TO DISPLACE ALL MUD FROM LATERAL ANNULAR, AT 750 BBL'S PUMPED PLUG LANDED, HOLD 4800 PSI FOR 10 MIN, BLEED OFF SAME, WITH ZERO RETURNS, WALK PRESSURE BACK UP TO 4800 PSI, BLEED OFF SAME, ZERO RETURNS, PULL OUT OF LINER TOP, WELL FLOWING SLIGHTLY, GET 7 BBL'S BACK, WELL STOPPED FLOWING AFTER RACKING BACK 2 STANDS, MAKE READY TO LAYDOWN DP. "PLUG DOWN & HOLDING / WELL SECURE AT ON 4/14/15";LAYDOWN 4 INCH DP. LD DP, ND, GET READY FOR RIG MOVE. Apr MD: 17,096 TVD: 10,999 FOOTAGE: MW: 0.0 LB PTD: 17,368 LD DP, LD WEATHERFORD ASSEMBLY, TIH WITH REMAINING DP, FINISH LD DP, CLEAR FLOOR, READY BOP FOR ND, ND BOP. LAYDOWN DP.;LAYDOWN SLICK PACKOFF ASSEMBLY, RELEASE WEATHEROFRD AT ON 4/14/15.;TIH WITH REMAINING DP & HWDP.;LAYDOWN DP.;GATHER ALL 4 INCH TOOLS, INVENTORY SAME & MAKE READY TO RETURN.;RIG DOWN, CHOKE & KILL LINES, FLOW-LINE, STANDPIPE, LOWER CAT WALK, READY BOP FOR ND.;MOVE IN & SPOT / RIG UP MONAHANS, HOLD PJSM WITH RIG & ND CREWS.;ND BOP, STAGE SURFACE EQUIPMENT FOR RIG MOVE. "RELEASE SUN DRILLING EQUIPMENT AT ON 4/15/15" FINISH ND, BACK HAUL SUN DRILLING EQUIP, RIG DOWN & GET READY FOR RIG MOVE.

11 Apr MD: 17,096 TVD: 10,999 FOOTAGE: MW: 0.0 LB PTD: 17,368 FINISH ND.;RIG DOWN & GET READY FOR RIG MOVE. FINISH ND, BACK HAUL SUN DRILLING EQUIPMENT, RIG DOWN & GET READY FOR RIG MOVE. "RELEASE ICD #208 TO THE UNIVERSITY 1-24 #2 AT ON 4/16/15" RELEASE RIG TO THE UNIVERSITY 1-24 #2, BEGIN RIG MOVE, NU TBG HEAD. Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 Apr MD: 17,096 TVD: 10,999 FOOTAGE: MW: 0.0 LB PTD: 17,368 NU & TEST TBG HEAD. NU 11 5K X 7 1/16 10K TBG HEAD, PACK OFF INNER VOID & TEST SAME TO 5000 PSI "TEST GOOD" TBG HEAD CAP 4 BOLTED HAND TIGHT, CLOSE ALL TBG & CSG VALVES, WELL HAS 0 PRESSURE. "ALL VALVES CLOSED / WELL SECURE 4/17/15" NONE. Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 Shut well in / wait on pulling unit MOVE IN RIG COIL TUBING UNIT - INSTALL FRAC VAVLE;WAIT ON PERF GUN;RUN PERF GUN ON COIL TUBING - TAG PICK UP SECON TIME- DROP BALL TO 16885' ' TOTAL OF 18 HOLES;RIG DOWN COIL TUBING UNIT - SHUT WELL IN Wait on pulling unit to run liner hager to cement liner Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 Wait on Pulling unit Wait on pulling unit Wait on Pulling unit Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 Waiting on Pulling unit Rig up Pulling unit - install bop Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 WAITING ON DAY LIGHT WAIT ON PULLING UNIT;MOVE IN RIG UP PULLING UNIT & RIG UP INSTALL BOP - UNLOAD 10500' 2 7/8 PH ' 2 3/8 PH 6 & /4 DRILL COLLARS - SHUT WELL IN OVER NIGHT P/U LINER HANGER TIH Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 WELL SHUT IN OVER NIGHT CALIPER DRILL COLLARS - STRAP COLLARS & 2 7/8" PH-6 TUBING - P/U LINER HANGER /4" DRILL COLLARS & 150 JOINTS TUBING - SWION FINISH RUNNING LINER HANGE & CEMENT Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 WELL SION FINISH TIH TAG LINNER 10140' -;RIG UP PUMP TRUCK PUMP DOWN TUBING PRESSURED UP TO 1500 AFTER PUMPING 10 BBLS - PULL OUT OF LINER TOP CIRCULATE TO SURFACE - STING INTO LINER TEST BACKSIED TOO 3500 PSI FOR 30 MINS - PULL OUT OF LINER L/D 1 JOINT OF TUBING - SWIOM DISCUSS NEXT STEP PROSSED AS PLANED

12 Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 WELL SHUT IN FOR WEEKEND PICK UP 2 JOINTS 2 7/8" PH6 TUBING STING IN TO LINER HANGER;ROTATE PIPE TO SET LINER HANGER - SET HANGE W/ 30,000LBS SITTING ON HANGER - WORK PIPE TO ENSURE GOOD SET ON HANGER - WHILE SETTING HANGER GOT 5" DOWN TRAVE - THAT SHOWES THAT WE GOT THE FIRST HANGER FULLEY SET.;TOOH STAND TUBBING - L/D /4" DRILL COLLARS - SHUT WELL IN FOR WEEKEND P/U BIT 2 3/8" TUBING TIH TAG BOTTOM CLEAN OUT AS NEEDED Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 SWION OPEN WELL - STRAP & 7PICK UP 228 JOINTS OF 2 3/8" PH ' TIH WITH 118 JOINTS OF 2 7/8" 2 7/8" PH6 - DID NOT SEE ANY DRAG WHEN WE WENT IN LINER TOP. SHUT DOWN FOR HIGH WIND.;SWION FINISH TIH TAG BOTTOM CIRCULATE HOLE CLEAN - TOOH Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 WELL SION FINISH TIH - TAG AT SLEEVE #7 ROTATE PIPE WITH TONGS - TIH 16944';RIG UP PUMP TRUCK PUMP WATER PSI - PUMPED 600 BBLS - HOLE CLEANED UP.;TOOH LAYING DOWN WORK STRING - SWION FINISH L/D WORK STRING - N/P BOP - INSTALL FRAC VAVLE - RIG DOWN MOVE OUT Apr MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 RIG SUPERVISOR: Tyler Dupriest PBTD: TOOH work string TOOH work string TOOH work string, RDMO May MD: TVD: FOOTAGE: MW: 0.0 LB PTD: 17,368 RIG SUPERVISOR: Tyler Dupriest PBTD: POOH and lay DN TBG. Rig up wireline to log well POOH and lay down work string. RDMO;Rig up wireline for bon log. RIH w/ wireline and log well. 2038'. Top of 3198'. RDMO RDMO PU and wireline. Rig up for frac WellEz Information Management, LLC. All rights reserved

APPROACH OPERATING LLC. RIG: Latshaw rig #22 KB: 28

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