APPROACH OPERATING LLC. RIG: Latshaw rig # 22 KB: 28
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- Emery Fletcher
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1 MORNING DRILLING REPORT Date: 6/5/2013 Day: 1 Present Operation: Drilling 12 1/4" hole with bit # 1 Depth: 609 Footage: 569 Rot. Hrs.: 6 Cum Rot Hrs: 6 Daily ROP: Brief Description Of Operations: Rig up back yard, rig up floor and front yard, nipple up conductor and flow line to pits, pick up BHA, make up bit, drilling from , Wireline survey at , trip out to unplug bit, drilling from , wireline survey at , drilling from Spud well at 930 pm
2 MORNING DRILLING REPORT Date: 6/6/2013 Day: 2 Present Operation: Waiting on cement, cutting conductor to weld on casing head Depth: 1260 Footage: 651 Rot. Hrs.: 6.5 Cum Rot Hrs: 12.5 Daily ROP: Brief Description Of Operations: Drilling 12 1/4" hole with bit #1 from , wireline survey at , drilling from , wireline survey at , drilling from , service Top Drive, drilling from , ( TD 1260 at 2 pm ), pump sweeps, work pipe, and condition hole to run 9 5/8" casing, trip out of hole, lay down 3-8" DCs, shock sub and bit, rig up casing tools, run casing, circulate casing on bottom with rig pump, rig down casing tools, rig up Baker Hughes, cement casing, *Bump Plug at 1130 pm , CIRCULATED 57 sacks to reserve, WOC, nipple down conductor, cut off conductor flange and make ready to weld on casing head.
3 MORNING DRILLING REPORT Date: 6/7/2013 Day: 3 Present Operation: testing bop w/ Monahans tester. Depth: 1260 Footage: 0 Rot. Hrs.: 0 Cum Rot Hrs: 12.5 Daily ROP: ##### Brief Description Of Operations: install weld on head, wait on repaired bop eq,replace rental bop, nu bop and test bop 2000 high/ 250 low...
4 MORNING DRILLING REPORT Date: 6/8/2013 Day: 4 Present Operation: dirc drlg rotate and slide 8 3/4 hole Depth: 2102 Footage: 842 Rot. Hrs.: 9 Cum Rot Hrs: 21.5 Daily ROP: Brief Description Of Operations: Finish testing bop and choke manifold 2000 high/250 low, test floor valves and mud lines 5000 high/ 250 low pu dirc tools and tih, tag 1191, drlg float eq and drlg out to shoe 1255, circ hole clean and ru multi shot and run gyro, dirc drlg rotate and slide f/ 1260 to 2102.
5 MORNING DRILLING REPORT Date: 6/9/2013 Day: 5 Present Operation: dirc drlg rotate and slide 8 3/4 hole Depth: 5266 Footage: 3164 Rot. Hrs.: 23.5 Cum Rot Hrs: 45 Daily ROP: Brief Description Of Operations: dirc drlg rotate and slide f/ 2102 to Service rig. Dirc drlg rotate and slide f/ 3387 to 5266.
6 MORNING DRILLING REPORT Date: 6/10/2013 Day: 6 Present Operation: dirc drlg 8 3/4 hole ( build curve ) Depth: 6097 Footage: 831 Rot. Hrs.: 14.5 Cum Rot Hrs: 59.5 Daily ROP: Brief Description Of Operations: dirc drlg rotate and slide f/ 5266 to 5738, pump sweeps and circ hole clean, pooh and ld dcs and dirc tools, pu bit #3 and dirc tools and tih to build curve. Dirc drlg rotate and slide f/ 5738 to 6097.
7 MORNING DRILLING REPORT Date: 6/11/2013 Day: 7 Present Operation: Rotary / slide drilling with bit # 3 Depth: 6786 Footage: 689 Rot. Hrs.: 23.5 Cum Rot Hrs: 83 Daily ROP: Brief Description Of Operations: Rotary / slide drilling from , service rig and top drive, rotatry / slide drilling from
8 MORNING DRILLING REPORT Date: 6/12/2013 Day: 8 Present Operation: DT- Latshaw 22 to change out travelling blocks Depth: 6818 Footage: 32 Rot. Hrs.: 1 Cum Rot Hrs: 84 Daily ROP: 32 Brief Description Of Operations: Rotate/ slide drilling from , pump sweeps, condition hole, trip out of hole, lay down curve assembly, pick up lateral assembly, scribe motor, change trash pump hoses from inside reserve to outside reserve, trip in hole to shoe at 1151, slip and cut drilling line, *DT- Latshaw to wait on crane and change out travelling blocks.
9 MORNING DRILLING REPORT Date: 6/13/2013 Day: 9 Present Operation: Rotary / slide drilling with bit # 4 Depth: 6943 Footage: 125 Rot. Hrs.: 5 Cum Rot Hrs: 89 Daily ROP: 25 Brief Description Of Operations: DT- Latshaw 22, change out travelling blocks, service rig, trip in hole with lateral assembly, rotary / slide drilling with bit # 4 from
10 MORNING DRILLING REPORT Date: 6/14/2013 Day: 10 Present Operation: Rotary / slide drilling with bit # 4 Depth: 8910 Footage: 1967 Rot. Hrs.: 20 Cum Rot Hrs: 109 Daily ROP: Brief Description Of Operations: Rotary / slide drilling from , service rig and top drive, rotary / slide drilling from , pump sweeps, work pipe for clean up cycle, rotary / slide drilling from Top of curve at Bottom of curve at 6944
11 MORNING DRILLING REPORT Date: 6/15/2013 Day: 11 Present Operation: dirc drlg rotate and slide 8 3/4 hole Depth: Footage: 1832 Rot. Hrs.: 19.5 Cum Rot Hrs: Daily ROP: Brief Description Of Operations: dirc drlg rotate and slide f/ 8910 to Perform a clean up cycle. Dirc drlg rotate and slide f/ 9620 to perform a clean up cycle. Dirc drlg rotate and slide f/ to
12 MORNING DRILLING REPORT Date: 6/16/2013 Day: 12 Present Operation: circ hole 8800 Depth: Footage: 657 Rot. Hrs.: 6.5 Cum Rot Hrs: 135 Daily ROP: Brief Description Of Operations: dirc drlg rotate and slide f/ to 10835, perform clean up cycle, dirc drlg rotate and slide f/ to perform clean up cycle, pooh to change motor, Ld bit #4 and motor, pu bit # 5 and fresh motor, MWD tools and fresh agitator, tih, wash to 8800 and circ hole clean to get prior sweeps out of hole.
13 MORNING DRILLING REPORT Date: 6/17/2013 Day: 13 Present Operation: pump sweeps and perform clean up Depth: Footage: 1224 Rot. Hrs.: 18.5 Cum Rot Hrs: Daily ROP: Brief Description Of Operations: wash to bottom and pump sweep and circ sweep out. Dirc drlg rotate and slide f/ to 11872, service rig, dirc drlg rotate and slide f/ to 12059, pump sweeps and perform clean up cycle, dirc drlg f/ to 12623
14 MORNING DRILLING REPORT Date: 6/18/2013 Day: 14 Present Operation: dirc drlg rotate and slide 8 3/4 hole Depth: Footage: 1066 Rot. Hrs.: 20 Cum Rot Hrs: Daily ROP: 53.3 Brief Description Of Operations: pump sweeps and perform clean up cycle, dirc drlg rotate and slide f/ to 13282, pump sweeps and perform clean up cycle,dirc drlg rotate and slide f/ to 13689
15 MORNING DRILLING REPORT Date: 6/19/2013 Day: 15 Present Operation: Pumping sweeps, work pipe and condition hole to run 5 1/2" casing Depth: Footage: 1054 Rot. Hrs.: 17 Cum Rot Hrs: Daily ROP: 62 Brief Description Of Operations: Rotary / slide drilling from , service rig and top drive, pump sweeps / clean up cycle, rotary / slide drilling from , pump sweeps / clean up cycle, rotary / slide drilling from (TD 14,743 at 4am ), pump sweeps,clean and condition hole to run 5 1/2" casing.
16 MORNING DRILLING REPORT Date: 6/20/2013 Day: 16 Present Operation: Running 5 1/2" casing Depth: Footage: 0 Rot. Hrs.: Cum Rot Hrs: Daily ROP: ##### Brief Description Of Operations: Pump sweeps, circulate and condition hole to run 5 1/2" casing, spot bead pill on bottom, pump out 10 stands, trip out of hole, spot beads at 11,000 and 9,000, lay down and load out directional tools, pull wear bushing, rig up casing tools, safety meeting, running 5 1/2" casing at report time.
17 MORNING DRILLING REPORT Date: 6/21/2013 Day: 17 Present Operation: Nipple down BOP stack Depth: Footage: 0 Rot. Hrs.: Cum Rot Hrs: Daily ROP: ##### Brief Description Of Operations: Complete running casing, rig down casing tools, rig up Baker Hughes, burst floatation tool with 3377 psi, circulate bottom up, drop Davis Lynch "blue plug", shear with 3279 psi, cement casing with Baker Hughes, bump plug at 1030 pm , circulated 224 sacks to reserve pit, rig down Baker Hughes, load out cementing equipment, lay down mouseholes, nipple down flowline, nipple down BOPs, hang stack, set slips, cut off casing, set stack down, nipple down stack to install tubing head. 5 1/2" shoe set at
18 MORNING DRILLING REPORT Date: 6/22/2013 Day: 18 Present Operation: Repairs to Wrangler catwalk Depth: Footage: Rot. Hrs.: Cum Rot Hrs: Daily ROP: ##### Brief Description Of Operations: Split BOP stack to lay down for rig move, rig down valves off mud cross, make final cut on casing, install tubing head and test with 5000 psi for 10 min, rig down stack winches, change elevators and bales, install 90 mousehole, lay down DP, service rig, lay down DP, rig up lay down line and lay down DP manually, *DT Latshaw- to repair Wrangler catwalk with technician / mechanic.
19 MORNING DRILLING REPORT Date: 6/23/2013 Day: 19 Present Operation: rig down waiting on trucks for rig move Depth: Footage: 0 Rot. Hrs.: Cum Rot Hrs: Daily ROP: ##### Brief Description Of Operations: finish repairs to pipe wrangler, finish ld drlg string using mouse hole,break subs off of top drive to allow inspection of top drive and subs. rig down and wait on trucks to move rig. rig 18: Final report.
APPROACH OPERATING LLC. RIG: Latshaw rig #22 KB: 28
MORNING DRILLING REPORT Date: 8/18/2013 Day: 1 Present Operation: waiting on daylight to finish rig move Depth: Footage: Rot. Hrs.: Cum Rot Hrs: 0 Daily ROP: ##### Brief Description Of Operations: move
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