MORNING DRILLING REPORT

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APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/13/2011 Day # 1 Well Name University 42-21 #1 H County Crockett Present Operation Mist drlg. 17 1/2'' hole Depth 800 Ft. / Day 760 Rotating Hours 16 Ttl. Rotating Hrs. 16 Brief Description Of Operations Work on top drive.rig inspection.pickup BHA.mist drlg. 17 1/2'' hole F/ 40 to 360.Service top drive.mist drlg. F/ 360 to 593. run WLS @ 500' 1.26*.Mist drlg. F/ 593 to 800 Spud @ 1;00pm 3-12-2011 Lost circulation @ 500' Daily Cost: $237,933 Accumulator Pressure: PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/14/2011 Day # 2 Well Name University 42-21 #1 H County Crockett Present Operation top out cement Depth 930 Ft. / Day 130 Rotating Hours 2 Ttl. Rotating Hrs. 18 Brief Description Of Operations Mist drlg. F/ 800 to 857.Break kelly saver sub.trip out of hole.change out die on backup wrench.trip in hole. Mist drlg. F/857 to930.load hole with drillcat polymer.trip out of hole.rigup casing crew and run 22 joint 13 3/8'' casing set at 925.28 circulate and rig down laydown machine.rigup Halliburton and cement.wait on cement. Run temp. survey top of cement @ 350. top out wih hallibuton. Plug down @ 10;30pm 3-13-2011 Daily Cost: $62,063 Accumulator Pressure: PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/15/2011 Day # 3 Well Name University 42-21 #1 H County Crockett Present Operation drlg. 12 1/4'' hole Depth 1489 Ft. / Day 559 Rotating Hours 6 Ttl. Rotating Hrs. 24 Brief Description Of Operations Top out cement.cutoff 13 3/8'' casing and weld on wellhead & test to 500psi.nipple up BOP and choke manifold. Test BOP and choke manifold with Monahans to 3000psi,test csing to 1000psi.Trip in hole with bit #3.Drlg cement and float equipment. drlg. 12 1/4'' hole F/ 930 to 1489 Daily Cost: $104,167 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/16/2011 Day # 4 Well Name University 42-21 #1 H County Crockett Present Operation drlg. 12 1/4'' hole Depth 3108 Ft. / Day 1619 Rotating Hours 22 1/2 Ttl. Rotating Hrs. 46 1/2 Brief Description Of Operations Drlg. F/ 1489 to 1583.Run WLS @ 1500 0.75*,1000 1.43*.Drlg. F/ 1583 to 1869.Service rig.drlg. F/ 1869 to 2059. Run WLS @ 2000 misrun. Drlg. F/ 2059 to 2154. Run WLS @ 2000 0.63*.Drlg. F/ 2154 to 2535.Run WLS @ 2500 1.44*.Drlg. F/ 2535 to 3108. Daily Cost: $48,667 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/17/2011 Day # 5 Well Name University 42-21 #1 H County Crockett Present Operation Cement 9 5/8'' casing Depth 3833 Ft. / Day 725 Rotating Hours 7 Ttl. Rotating Hrs. 53 1/2 Brief Description Of Operations WLS @ 3000 1.19*.Drlg.F/ 3108 to 3585.Service rig & WLS @ 3500 0.18*.drlg. F/ 3585 to 3833.Pump sweeps and circulate to run gyro. Run gyro every 200ft.Trip out of hole,rigup laydown machine and laydown collars.rigup casing crew and run 85 joints 9 5/8'' 40# casing set 2 3833.62.circulate and rigdown laydown machine.cement with Halliburton. TD @ 2;30pm 3-16-2011 Plug down @ 6;30am 3-17-2011 Daily Cost: $158,480 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/18/2011 Day # 6 Well Name University 42-21 #1 H County Crockett Present Operation Test BOP Depth 3833 Ft. / Day Rotating Hours Ttl. Rotating Hrs. 53 1/2 Brief Description Of Operations Top out cement with Halliburton.rigdown halliburton.nipple down BOP.Set slips,cutoff casing, install B section and test.nipple up BOP.Wait on Monahans.Inspect derrick and top drive for droped part,part off of upper kelly valve controller.test BOP,choke,mud lines,floor valves and casing.replace 4'' valve on choke Daily Cost: $44,021 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/19/2011 Day # 7 Well Name University 42-21 #1 H County Crockett Present Operation Wait on parts for rotary clutch Depth 3833 Ft. / Day Rotating Hours Ttl. Rotating Hrs. 53 1/2 Brief Description Of Operations Test 4'' valve on choke manifold.get floor and ground ready to pickup BHA ( safety).pickup Directional tools and surfuce test.work on rotary clutch and wait on parts. Daily Cost: $16,735 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/20/2011 Day # 8 Well Name University 42-21 #1 H County Crockett Present Operation Rotate drlg. Depth Ft. / Day 4226 393 Rotating Hours 8 1/2 Ttl. Rotating Hrs. 62 Brief Description Of Operations to 4226 Wait on rotart clutch part.test MWD tools. Trip in hole.drlg. Cement and float equipment.rotate drlg. F/ 3833 Daily Cost; $19,881 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/21/2011 Day # 9 Well Name University 42-21 #1 H County Crockett Present Operation slide drlg. Depth 5380 Ft. / Day 1154 Rotating Hours 24 Ttl. Rotating Hrs. 86 Brief Description Of Operations Rotate drlg. F/ 4226 to 5290. Slide drlg. f/ 5290 to 5380 Daily Cost: $31,451 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/22/2011 Day # 10 Well Name University 42-21 #1 H County Crockett Present Operation slide drlg. Depth 5800 Ft. / Day 420 Rotating Hours 15 Ttl. Rotating Hrs. 101 Brief Description Of Operations Slide drlg. F/ 5380 to 5382.Trip out of hole.change out motor,bit and test MWD.service top drive.trip in hole. Slide drlg. F/ 5382 to 5528.Calibrate block tracking.slide drlg. F/ 5528 to 5800 Daily Cost: $62,751 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/23/2011 Day # 11 Well Name University 42-21 #1 H County Crockett Present Operation trip out of hole Depth 6316 Ft. / Day 516 Rotating Hours 18 1/2 Ttl. Rotating Hrs. 119 1/2 Brief Description Of Operations Trip out of hole. Service top drive.slide drlg. F/ 5800 to 6224. Rotate drlg. F/ 6224 to 6316.Circulate and cond. Hole for trip. Daily Cost: $39,110 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/24/2011 Day # 12 Well Name University 42-21 #1 H County Crockett Present Operation Rotate drlg. Depth Ft. / Day 7264 948 Rotating Hours 15 1/2 Ttl. Rotating Hrs. 135 Brief Description Of Operations test tools.rotate drlg. F/ 6316 to 7264 Trip out of hole and change out motor,bit and MWD tools.service rig.replace MWD tools and test.trip in hole and Daily Cost: $ 41,900 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/25/2011 Day # 13 Well Name University 42-21 #1 H County Crockett Present Operation Rotate & slide drlg.. Depth Ft. / Day 8350 1086 Rotating Hours 21 1/2 Ttl. Rotating Hrs. 156 1/2 Brief Description Of Operations Rotate & slide drlg.service rig.rotate & slide drlg. Circulate and clean hole. Rotate and slide drlg. Daily Cost: $35,292 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Well Name Present Operation Depth University it 42-21 21 #1 H Rotate & slide drlg.. Ft. / Day 9660 1310 Date 3/26/2011 Day # 14 County Rotating Hours 21 1/2 Crockett Ttl. Rotating Hrs. 178 Brief Description Of Operations Rotate and slide drlg. Circulate.rotate and slide drlg. Service rig. Rotate and slide drlg. Circulate.rotate and slide drlg. Accumulator Pressure: 1900 PSI Notify RRC of Spud @ 6;00pm 3-10-2011 job #1843 ( IVY ) Nozzles Bit Bit Make Type Serial 32nds Depth Depth Total Hours on Ft./Hr. Bit RPM Number Size Number In Out Footage Bit Weight Run # 1 2 3 5 83/4'' Ulterra Z25RS CW416 3x22 322 5382 6316 934 32 1/2 28.7 30-40 slide 6 8 3/4'' Varel VM616H 4001133 8x18 6316 3344 58 1/2 57.1..22 80 Compressors 3 Booster(s) 1 CFM 3000 Nitrogen Unit on line at O2% Dusting (y/n) N Misting with: F/W bbls. 25 Foamer gph 5 Shale Treat gal./hr. Corrosion Inhibitor gal./hr. Hydraulics # 1 pump ( @ 95% - GPS = 4.409 - BPS = 0.1050 ) & # 2 pump @ 95% - GPS = 4.409 - BPS = 0.1050 Pump # 1 Stroke Liners SPM GPM Pump Pressure Nat. oilwell FB 1600 12 6'' 65 272 1900 off bot./2000 Pump#2 Stroke Liners SPM Nat. oilwell FB 1600 12 6'' 65 Mud Properties Wt. Fun'l Filtrate Cake Chlorides Vis. PV/YP Gels PH CC/30 min. 32nds. Pm pf/mf PPM HT API GPM Pump Pressure 272 Calcium % % % Vis. PPM Sand Solids Oil Out 9.8 30 10 152000 FUEL Rig Diesel - " 23 Air Diesel - " 25 Propane - % Gallons of Diesel delivered Remarks Directional Surveys WLS 1 2 3 4 5 Depth 8656 8845 9036 9226 9321 Angle 89.1*-2.10azm 90.4*-359.8azm 90.*-358.4azm 89.*-3.10azm 88.6*-3.00azm Bottom Hole Assembly (BHA) No Change (see prior report) Tool Description * New BHA Drill Pipe Size OD (in) Wt. ID (in) 6 7 9417 89.8*-3.70azm 89.8*-2.30azm Grade Length (ft) 9512 1-PDC 8 3/4'' 1 1-1.83* motor 63/4'' 26.34 1- float sub 6 5/16'' 2.32 1- pony flex NMDC 6'' 8.34 1-UBHO 63/16'' 272 2.72 1-NMDC 6 1/8'' 28.8 1- flex NMDC 6 5/8'' 31.09 Brine on hand 500 Barrels Freshwater on hand 1000 Barrels Mud on hand 800 PU wt. 200 Barrels Slack Off Wt. 110 K Rotating Wt. - 150 K BHA 100.61

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Well Name University it 42-21 21 #1 H Present Operation Rotate & slide drlg.. Depth 10560 Ft. / Day Date 900 3/27/2011 Day # 15 County Rotating Hours 21 Crockett Ttl. Rotating Hrs. 199 Brief Description Of Operations Rotate and slide drlg. Circulate and cond. Hole.rotate and slide drlg.service rig. Rotate and slide drlg. Jet shale pit. Rotate and slide drlg. Accumulator Pressure: 1900 PSI Notify RRC of Spud @ 6;00pm 3-10-2011 job #1843 ( IVY ) Nozzles Bit Bit Make Type Serial 32nds Depth Depth Total Hours on Ft./Hr. Bit RPM Number Size Number In Out Footage Bit Weight Run # 1 2 3 5 83/4'' Ulterra Z25RS CW416 3x22 322 5382 6316 934 32 1/2 28.7 30-40 slide 6 8 3/4'' Varel VM616H 4001133 8x18 6316 4244 79 1/2 53.3..22 80 Compressors 3 Booster(s) 1 CFM 3000 Nitrogen Unit on line at O2% Dusting (y/n) N Misting with: F/W bbls. 25 Foamer gph 5 Shale Treat gal./hr. Corrosion Inhibitor gal./hr. Hydraulics # 1 pump ( @ 95% - GPS = 4.409 - BPS = 0.1050 ) & # 2 pump @ 95% - GPS = 4.409 - BPS = 0.1050 Pump # 1 Stroke Liners SPM GPM Pump Pressure Nat. oilwell FB 1600 12 6'' 65 272 2800 off bot./2850 Pump#2 Stroke Liners SPM GPM Pump Pressure Nat. oilwell FB 1600 12 6'' 65 272 Mud Properties Wt. Fun'l Filtrate Cake Chlorides Calcium % % % Vis. Vis. PV/YP Gels PH CC/30 min. 32nds. Pm pf/mf PPM PPM Sand Solids Oil Out HT API 9.8 29 10 160000 FUEL Rig Diesel - " 54 Air Diesel - " 25 Propane - % Gallons of Diesel delivered 7000 Remarks Rot. Tq. Off bottom;5000=rot. Tq.on bottom;11700 WLS 1 2 Depth Angle 9893 88.7*-359.60azm 9988 88.5*-358.7azm 10083 89.2*-358.azm 10178 88.9*-359.3azm 10274 88.88-358.2azm 10368 89.1*-357.3azm 10463 88.7*-357.5azm Bottom Hole Assembly (BHA) No Change (see prior report) Tool Description 1-PDC * Directional Surveys 3 4 5 6 7 New BHA Drill Pipe Size Wt. OD (in) ID (in) 8 3/4'' 1-1.83* motor 63/4'' Grade Length (ft) 1 26.34 1- float sub 6 5/16'' 2.32 1- pony flex NMDC 6'' 8.34 1-UBHO 63/16'' 272 2.72 1-NMDC 6 1/8'' 28.8 1- flex NMDC 6 5/8'' 31.09 Brine on hand 500 Barrels Freshwater on hand 1000 Barrels Mud on hand 500 Barrels PU wt. 200 Slack Off Wt. K Rotating Wt. - 154 K BHA 100.61

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Well Name Present Operation Depth University it 42-21 21 #1 H Down wait on electrician Ft. / Day 10673 113 Date 3/28/2011 Day # 16 County Rotating Hours 7 1/2 Crockett Ttl. Rotating Hrs. 206 1/2 Brief Description Of Operations Rotate and slide drlg. Service rig.rotate and slide drlg. Trip out of hole f/ motor.work on ST80.trip out of hole. laydown bad motor and pickup new motor and test.trip in hole and pickup agitator at 3054'.test MWD tool at 3933'. Wait on electrician Accumulator Pressure: 1900 PSI Notify RRC of Spud @ 6;00pm 3-10-2011 job #1843 ( IVY ) Nozzles Bit Bit Make Type Serial 32nds Depth Depth Total Hours on Ft./Hr. Bit RPM Number Size Number In Out Footage Bit Weight Run # 1 2 3 7 83/4'' Varel DE616 4000811 6x20 620 10673 6 8 3/4'' Varel VM616H 4001133 8x18 6316 10673 4357 87 50..22 80 Compressors 3 Booster(s) 1 CFM 3000 Nitrogen Unit on line at O2% Dusting (y/n) N Misting with: F/W bbls. 25 Foamer gph 5 Shale Treat gal./hr. Corrosion Inhibitor gal./hr. Hydraulics # 1 pump ( @ 95% - GPS = 4.409 - BPS = 0.1050 ) & # 2 pump @ 95% - GPS = 4.409 - BPS = 0.1050 Pump # 1 Stroke Liners SPM GPM Pump Pressure Nat. oilwell FB 1600 12 6'' 65 272 2800 off bot./2850 Pump#2 Stroke Liners SPM Nat. oilwell FB 1600 12 6'' 65 Mud Properties Wt. Fun'l Filtrate Cake Chlorides Vis. PV/YP Gels PH CC/30 min. 32nds. Pm pf/mf PPM HT API GPM Pump Pressure 272 Calcium % % % Vis. PPM Sand Solids Oil Out 9.8 29 10 160000 FUEL Rig Diesel - " 45 Air Diesel - " 25 Propane - % Gallons of Diesel delivered Remarks Directional Surveys WLS 1 2 3 4 5 6 7 Depth 10558 Angle 88.8*-358.2azm Bottom Hole Assembly (BHA) No Change (see prior report) Tool Description 1-PDC * New BHA Drill Pipe Size OD (in) 8 3/4'' 1-1.83* motor 6 3/4'' Wt. Grade ID (in) Length (ft) 1 25.97 1- float sub 6 5/16'' 2.32 1- pony flex NMDC 6'' 8.34 1-UBHO 63/16'' 272 2.72 1-NMDC 6 1/8'' 28.8 1- flex NMDC 6 5/8'' 31.09 1agitator ---1 shock sub 6 3/4'' 6 5/8'' 20.9 Brine on hand 500 Barrels Freshwater on hand 1000 Barrels Mud on hand 500 Barrels PU wt. 200 Slack Off Wt. K Rotating Wt. - 154 K BHA 121.14

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date Day # 3/29/2011 17 Well Name University 42-21 #1 H County Crockett Present Operation rotate and slide drlg. Depth 11155 Ft. / Day 482 Rotating Hours 11 Ttl. Rotating Hrs. 217 1/2 Brief Description Of Operations wait on electrican.trip in hole. Work on hy-drum clutch.trip in hole.wash to bottom F/ 9579 to 10148.adjust brakes. wash to bottom F/10148 to 10673.work on pumps.rotate and slide drlg.change out swab on pump. Rotate and slide drlg. Change out viberator hose. Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date Day # 3/30/2011 18 Well Name University 42-21 #1 H County Crockett Present Operation trip out of hole for motor Depth 11920 Ft. / Day 765 Rotating Hours 19 Ttl. Rotating Hrs. 236 1/2 Brief Description Of Operations Rotate and slide drlg.service rig.rotate and slide drlg.circulate and clean hole.trip out of hole for motor Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 3/31/2011 Day # 19 Well Name University 42-21 #1 H County Crockett Present Operation rotate and slide drlg. Depth Ft. / Day 12200 280 Rotating Hours 7 1/2 Ttl. Rotating Hrs. 244 Brief Description Of Operations trip out of hole.laydown motor,pickup new motor and test.trip in hole to casing shoe.test agitator,and MWD tools. slip and cut drlg. Line.trip in hole.ream F/ 10726 to 11920.rotate and slide drlg. f/ 11920 to 12200 Daily Cost: $49,599 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 4/1/2011 Day # 20 Well Name University 42-21 #1 H County Crockett Present Operation Laydown drillpipe Depth Ft. / Day 550 Rotating Hours 10 1/2 Ttl. Rotating Hrs. 254 1/2 Brief Description Of Operations Rig up laydown machine.laydown drillpipe. Rotate and slide drlg. F/ 12200 to.circulate and cond. Hole.Trip out of hole to 5200'.wait on laydown machine. TD @ 4;30pm 3-31-2011 Daily Cost: $29,982 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 4/2/2011 Day # 21 Well Name University 42-21 #1 H County Crockett Present Operation Run 5 1/2'' 17# casing Depth Ft. / Day Rotating Hours Ttl. Rotating Hrs. 254 1/2 Brief Description Of Operations Laydown drillpipe.laydown MWD tools and motor.trip in hole.laydown drillpipe.trip in hole.laydown drillpipe Rigup CRT tool to run casing.run 5 1/2'' 17# P110 casing. Daily Cost: $29,860 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 4/3/2011 Day # 22 Well Name University 42-21 #1 H County Crockett Present Operation Nipple down Depth Ft. / Day Rotating Hours Ttl. Rotating Hrs. 254 1/2 Brief Description Of Operations Ran 300 joints 5 1/2'' 17# P110 casing set at 12744.42.Circulate and wait on cement head f/ halliburton. Cement 5 1/2'' casing with halliburton.nipple down to set slips on casing. Daily Cost: $428,029 Plug down @ 2;30am 4-3-2011 Accumulator Pressure: 1900 PSI

APPROACH OPERATING LLC. RIG - Nabors # 714 KB - '22 MORNING DRILLING REPORT Date 4/4/2011 Day # 23 Well Name University 42-21 #1 H County Crockett Present Operation Rig Down Depth Ft. / Day Rotating Hours Ttl. Rotating Hrs. 254 1/2 Brief Description Of Operations Nipple Down BOP. Set slips and cut off casing. Nipple up Tubing head and Jet and clean pits. Rig Down. Daily Cost: $21,455 Accumulator Pressure: PSI Released Rig @ 6:00am 4/4/2011

1 UNIVERSITY 42-21 1 H 11-813 APRIL 14,2011 12744' LOG WELL 18 4-1/2" 11.6# N-80 Notched Collar @ Pkr. Set @ CIBP Set @ CIBP Set @ MOVE IN RIG UP E+P WIRELINE TO LOG WELL.RUN IN HOLE WITH GAMA-RAY, CASING COLLAR AND CEMENT BOND LOGGING TOOLS. RUN DOWN TO 6100' PULL LOGS UP TO 3500'. FOUND TOP OF CEMENT AT ' AND SHORT JOINT FROM 5527' TO 5547'. PULL OUT OF HOLE RIG E+P WIRELINE DOWN FROM WELL. BWTR BWR BWUL 0 Daily Cost $12,040.00 Cum Completion Cost: $12,040.00

2 UNIVERSITY 42-21 1 H 11-813 4.15.11 12744' RUN TBG 18 4-1/2" 11.6# N-80 2 3/8" 4.7# N-80 Notched Collar @ Pkr. Set @ CIBP Set @ CIBP Set @ MIRU NABORS WELL SERVICES. PICK UP 4 3/4" DRILL BIT, RIH W/ 64 JTS OF PH-6 TBG AND 266 JTS OF P-110 TBG. TBG STOP FALLING IN HOLE AT 11495'. DECIDED TO SHUT DOWN OVERNIGHT BWTR BWR BWUL 0 Daily Cost $4,500.00 Cum Completion Cost: $16,540.00

3 UNIVERSITY 42-21 1 H 11-813 4.18.11 12744' RUN TBG 22 5 1/2" 17# N 80 2 3/8" 4.7# N-80 400 Notched Collar @ Pkr. Set @ CIBP Set @ 12495' CIBP Set @ MOVE IN RIG UP WEATHERFORD POWER SWIVEL AND NABORS PUMP TRUCK. CONTINUE TO RUN IN HOLE WITH 300-JTS OF 2-7/8" CS HYDRILL TUBING. INSTAL -OVER AND RUN IN HOLE WITH 36-JTS OF 2-7/8" 8-RD UP SET TUBING.MIED FR MATERIAL AND CIRCULATED HOLE. TOTAL TUBING RUN 64-JTS OF PH 6 = 2034' 2034' 300-JTS OF CS HYDILL =9351 11385' 36-JTS OF 8-RD UP-SET = 1111' 12496' RIG POWER SWIVEL DOWN FROM WELL. RIG UP B- J SERVICES TO PICKLE TUBING. PUMP 500-GALS OF 15% NEFE HCL ACID DOWN TUBING. FLUSH ACID DOWN TUBING AND BACK THROUGH CASING WITH 290-BBLS OF 5% KCL WATER. RIG B-J SERVICES DOWN FROM WELL. PULL 20-JTS OF TUBING, NIPPLE DOWN B-O-P AND TUBING HANGER. NIPPLE UP NEW TUBING HANGER WITH 7-1/8" 10-K FLANGE. HANG TUBING IN WELL HEAD WITH WRAP AROUND. SHUT WELL IN OVER NIGHT. Max Torque - 2500 Max drag - 60,000 before FR - 22,000 after FR BWTR BWR BWUL 0 Daily Cost $15,550.00 Cum Completion Cost: $30,790.00

4 UNIVERSITY 42-21 1 H 11-813 4.19.11 12744' RUN TBG 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 Notched Collar @ Pkr. Set @ CIBP Set @ 12495' CIBP Set @ MET BJ SERVICES ON LOCATION. RIG UP ON TBG, PRESSURE WELL TO 7500 PSI TO SLIDE SLEEVE AT 12602'. AFTER SEVERAL ATTEMPTS SLEEVE OPENED WITH 9000 PSI. MET IN OFFICE TO DISCUSS PRE FRAC PROCEDURES WITH MANAGEMENT AND HALIBURTON PERSONEL. ON LOCATION, PREPARE WELL TO BE ACIDIZED. HALIBURTON COULD NOT ACIDIZE WELL TODAY SHUT WELL IN OVERNIGHT. BWTR BWR BWUL 0 Daily Cost $8,300.00 Cum Completion Cost: $39,090.00

5 UNIVERSITY 42-21 1 H 11-813 4.20.11 12744' PERF WELL 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 Notched Collar @ Pkr. Set @ CIBP Set @ 12495' CIBP Set @ ON LOCATION, RIG UP APPROACH PUMP TRUCK TO WELL HEAD. PUMP 500 GALS OF 10% ACETIC ACID DOWN TBG AND DISPLACED ACID TO END OF TBG WITH 75 BBLS OF 5% KCL WATER. PULL TBG OUT OF HOLE LAYING DOWN. RIG UP HALIBURTON WIRELINE, PREPARED TO RUN IN HOLE WITH 3 1/8" CSG GUNS. CALLED IN TO FIND OUT WHEN PUMPTRUCKS WOULD BE ON LOCATION FOUND THAT THEY WOULD NOT BE ON LOCATION UNITIL 9:30 PM DECIDED TO SHUT DOWN OVER NIGHT. BWTR BWR BWUL 0 Daily Cost $5,550.00 Cum Completion Cost: $44,640.00

6 UNIVERSITY 42-21 1 H 11-813 4.21.11 12744' PERF 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 Notched Collar @ Pkr. Set @ CIBP Set @ 12495' CIBP Set @ ON LOCATION, RIG UP HALLIBURTON WIRELINE AND HALIBURTON PUMP TRUCK TO WELL HEAD. RIH W/ 3 1/8: CSG GUNS TO 6100'. START PUMPING WATER TO PUMP GUNS DOWN HOLE. PUMP MA INJECTION RATE OUT AT 8 BPM WITH 5200 PSI. PUMP RATE WAS NOT STRONG ENOUGH TO GUNS TO END OF TBG. DECIDED TO SHUT DOWN AND PULL GUN OUT OF HOLE. COULD NOT FIND PUMPS FROM OTHER SERVICE COMPANY'S, HAD TO SHUT DOWN. DECIDED TO LET HALLIBURTON PUMP GUNS DOWN WITH FRAC TRUCKS ON SATURDAY BEFORE STARTING FRAC JOB. SHUT WELL IN RIG DOWN HALLIBURTON AND NABORS WELL SERVICE DOWN FROM WELL. BWTR BWR BWUL 0 Daily Cost $2,500.00 Cum Completion Cost: $47,140.00

7 UNIVERSITY 42-21 1 H 11-813 4.22.11 12744' LOG AND PERF 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 Notched Collar @ Pkr. Set @ CIBP Set @ 12495' CIBP Set @ 12499' TO 12502' 12399' TO 12402' MIRU HALIBURTON FOR FRAC JOB. ATTENDED HALIBURTONS SAFETY MEETINGTHEN TESTED LINES TO 9000 PSI. RIH W/ GUNS, CEMENT BOND LOGS, AND PUMPING GUNS AT 12 BPM. HAD TO INCREASE RATE TO 15 BPM TO GET GUNS DOWN HOLE. SHOT PERFORATIONS AS FOLLOWS: 12499' TO 12502' WITH 6 SPF = 19 HOLES 12399' TO 12402' WITH 6 SPF = 19 HOLES 38 HOLES TOTAL CAME BACK OUT OF HOLE CLOSED IN WELL HEAD FOR NET DAY START. COMENTS: DOWN HOLE BLENDER NOT ON LOCATION YET AND STILL HAVE TO RIG UP 4 PUMPS FROM LAST SHOT WE LOG COMING OUT OF HOLE TO HAVE A MARKER TO GO BY WITH THE CSG TALLY. BWTR BWR BWUL 0 Daily Cost $1,040.00 Cum Completion Cost: $48,180.00

8 UNIVERSITY 42-21 1 H 11-813 4.24.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 Notched Collar @ Pkr. Set @ CIBP Set @ 12340' 12499' TO 12502' 12399' TO 12402' 12299' TO 12302' 12199' TO 12202' 12099' TO 12102' 12495' CIBP Set @ STAGE 1 PUMPED AS FOLLOWS: TOOK 6886PSI TO BREAK FORMATION 4.3BPM SPEAR HEADED 3,500GALS OF 15% NE HCL ACID TO TOP OF PERFS SHUT DOWN TO FI WELL HEAD STARTED BACK UP ON PAD AND WENT WITH REGULAR SCHEDULE FROM THAT POINT OF JOB TOTAL FLUID INJECTED=223,212GALS TOTAL SAND INJECTED=312,229LBS MA TREATING PSI=6970PSI AVG TREATING PSI=6087PSI MA INJECTION RATE=78.7BPM AVG INJECTION RATE=72BPM ISIP=2754PSI 5 MIN=2693PSI 10 MIN=2683PSI 15 MIN=2577PSI SHUT IN WELL RIGGED UP WIRE LINE TO SET PLUG AND PERF AS FOLLOWS: RAN TO 12,340' SET PLUG PERF WELL AT 12099' TO 12,102 WITH 6SPF=19HOLES 12199' TO 12202 WITH 6SPF=19HOLES 12299' TO 12302' WITH 6SPF=19HOLES 57HOLES TOTAL WIRE LINE CAME OUT OF HOLE SHUT IN WELL FOR OVERNITE BWTR BWR BWUL 0 Daily Cost $1,040.00 Cum Completion Cost: $49,220.00

UNIVERSITY 42-21 1 H 11-813 4.25.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 9 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 12495' STAGE2 STAGE 3 PUMPED AS FOLLOWS: TOOK 4578PSI TO BREAK FORMATION 4.3BPM SPEAR HEADED 3,500GALS OF 15% NE HCL ACID WITH BALL IN FRONT OF ACID MADE RATE ADJUSTMENTS FOR BALL TO HIT THEN STAGE INTO OUR PAD AND FOLLOW SCHEDULE TOTAL FLUID INJECTED=227,497GALS TOTAL SAND INJECTED=319,044LBS MA TREATING PSI=5969PSI AVG TREATING PSI=4393PSI MA INJECTION RATE=78.5BPM AVG INJECTION RATE=65BPM ISIP=2480PSI 5 MIN=2325PSI 10 MIN=2265PSI 15 MIN=2210PSI SHUT IN WELL RIGGED UP WIRE LINE TO SET PLUG AND PERF AS FOLLOWS: RAN TO 12,050' SET PLUG PERF WELL AT 11,799'' TO 11,802' WITH 6SPF=19HOLES 11,899' TO 11,902' WITH 6SPF=19HOLES 11,999' TO 12,002' WITH 6SPF=19HOLES 57HOLES TOTAL PUMPED AS FOLLOWS: TOOK 4265PSI TO BREAK FORMATION 5.3BPM PUMPED 3,500 GALS OF 15%NE HCL ACID BEHIND BALL WHEN BALL HIT MADE ADJUSTMENTS TO BE ON SCHEDULE AND PUMPED AS FOLLOWS: TOTAL FLUID INJECTED=224,574GALS TOTAL SAND INJECTED=312,144LBS MA TREATING PSI=6235PSI AVG TREATING PSI=4461PSI MA INJ=78BPM AVG RATE=62BPM ISIP=2373PSI 5 MIN=2170PSI 10 MIN=2088PSI 15 MIN=2032PSI RAN TO 11,760'' SET PLUG PERF WELL AT 11,499'' TO 11,502' WITH 6SPF=19HOLES (NET PAGE) BWTR 675283 BWR BWUL 675283 Daily Cost $1,040.00 Cum Completion Cost: $50,260.00

UNIVERSITY 42-21 1 H 11-813 4.25.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 9 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 12495' 11,599' TO 11602' WITH 6SPF=19 HOLES STAGE 4 11,699' TO 11,702' WITH 6SPF=19 HOLES 57 HOLES TOTAL TOOK 4873PSI TO BREAK FORMATION AT 6.2BPM FOLLOWED UP WITH 3,500GALS OF 15%HCL ACID MA TREATING PSI=6274PSI AVG TREATING PSI=4305PSI MA INJECTION RATE=79.1BPM AVG INJECTION RATE=60BPM TOTAL SAND INJECTED=316,234LBS TOTAL FLUID INJECTED=230,303.9GALS ISIP=2502PSI 5 MIN=2438PSI 10 MIN=2383PSI 15 MIN=2328PSI SHUT IN WELL WIND TO HIGH FOR CRANE SET UP FOR AM START BWTR 991517 BWR BWUL 991517 Daily Cost $1,040.00 Cum Completion Cost: $50,260.00

9 UNIVERSITY 42-21 1 H 11-813 4.25.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 12495' 10830 10879' to 11102' WENT IN HOLE WITH GUNS AND FRAC PLUG PUMPED GUNS DOWN AT 12BPM AND A AVG PSI OF 2,430PSI STAGE 5 STAGE 6 PLUG AND PERFORATIONS WENT AS FOLLOWS:PLUG SET @11,450' PERFS:11,199' 199' TO 11,202' WITH 6SPF=19HOLES 11,299' TO 11,302' WITH 6SPF=19HOLES 11,399' TO 11402' WITH 6SPF=19HOLES 57HOLES TOTAL DROPPED BALL CHASED IT WITH 3,500GALS OF 15% HCL ACID @ 20BPM SLOWED RATE DOWN WHEN BALL WAS GOING TO HIT ONCE BALL HIT ESTABLISHED RATE ACCORDING TO BREAK BACK THEN WENT WITH SCHEDULE AS FOLLOWS:MA TREATING PSI=6,224PSI AVG TREATING PSI=4,359PSI MA INJECTION RATE=80BPM AVG INJECTION RATE=65BPM TOTAL FLUID INJECTED=235,069GALS TOTAL SAND INJECTED=292,877LBS TOOK 3,881PSI TO BREAK FORMATION AT 10BPM (LOST ONE PUMP TOLD IT COULD BE FIED) ISIP=2,448PSI 5 MIN=2,300PSI 10 MIN=2,245PSI 15 MIN=2,200PSI WENT IN HOLE WITH GUNS AND FRAC PLUG PUMPED GUNS DOWN AT 12BPM AND A AVG PSI OF 2,270PSI PLUG AND PERFORATIONS WENT AS FOLLOWS:PLUG SET @11,150' PERFS:10,879' TO 10,882' WITH 6SPF=19HOLES 10,979' TO 10,982' WITH 6SPF=19HOLES 11,099' TO 11,102' WITH 6SPF=19HOLES 57HOLES TOTAL COMENTS:WE DID HAVE A MISS FIRE TOLD WIRE LINE TO COME OUT OF HOLE SLOW PLUG WAS STILL ON NET PAGE BWTR 1226586 BWR BWUL 1226586 Daily Cost $1,040.00 Cum Completion Cost: $51,300.00

9 UNIVERSITY 42-21 1 H 11-813 4.25.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 12340' 12050' 11760' 11450 11150 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 12495' 10830 10830 10879' to 11102' STAGE 6 TOOK 3,807PSI TO BREAK FORMATION AT 9BPM WE CHASED BALL WITH 3,500GALS OF 15% HCL ACID @ 15BPM SLOWED THE RATE DOWN TO 9BPM WHEN BALL WAS ABOUT TO HIT THEN CAME UP ON OUR RATE ACCORDING TO THE BREAKS IN FORMATION TO OUR SCHEDULED RATE AND FOLLOWED FRAC SCHEDULE AS FOLLOWS: MA TREATING PSI=5,867PSI AVG TREATING PSI=4,308PSI MA INJECTION RATE=79.9 AVG INJECTION RATE=63.0 TOTAL FLUID INJECTED=219,569GALS TOTAL SAND INJECTED=310,524LBS ISIP=2,458PSI 5 MIN=2,263PSI 10 MIN=2,211PSI 15 MIN=2,159PSI COMENTS:HP WAS SHORT MAKING ADJUSTMENTS AS WE WENT PUMPS GETTING HOT,LOSING ANTI FREEZE TURBO ON ONE PUMP ON FIRE AT ONE POINT WITH HALIBURTON CREW HAVING TO SHUT PUMP IN AND ATTEND TO PROBLEM.ON 4# SAND WE HAD TO BUMP RATE UP TO BREAK OVER HIGHER SAND CONS. BY DOING THIS PUMPS WERE GETTING OVERWORKED DUE TO LACK OF HP WE DID GET ALL SAND RAN RAN IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET FRAC PLUG @10,830' PUMPED GUNS IN @13BPM AVG PSI OF=2584PSI PERFS AS FOLLOWS: 10,579' TO 10,582' WITH 6SPF=19HOLES 10,679' TO 10,682' WITH 6SPF=19HOLES 10,779' TO 10,782' WITH 6SPF=19HOLES COMENTS: 57HOLES TOTAL PERFORATING WAS DELAYED DUE TO WIND,HALIBURTON WORKED ON PUMPS WAITING ON REPORT FROM THEM ABOUT HP FRAC WOULD BE DELAYED TILL THE AM BWTR 1446155 BWR BWUL 1446155 Daily Cost $1,040.00 Cum Completion Cost: $51,300.00

11 UNIVERSITY 42-21 1 H 11-813 4.27.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 12495' 10830 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 10879' to 11102' STAGE 7 TOOK 4,242PSI TO BREAK FORMATION AND SEAT BALL AT 10BPM FOLLOWED BY 3,500GALS OF 15% HCL ACID ONCE ACID ON MADE ADJUSTMENTS ON RATE TO GET MAIMUM BREAKS IN FORMATION THEN FOLLOWED FRAC SCHEDULE AS FOLLOWS: MA TREATING PSI=6,537PSI AVG TREATING PSI=4,367PSI ISIP=2,515PSI 5 MIN=2,389PSI MA INJECTION RATE=80BPM AVG INJECTION RATE=64BPM 10 MIN=2,355PSI 15 MIN=2,334PSI TOTAL FLUID INJECTED=223,032GALS TOTAL SAND INJECTED=312,876LBS RAN IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET PLUG @10,530' PERFS AS FOLLOW: 10,279' TO 10,282' WITH 6SPF =19HOLES 10,379' TO 10,382' WITH 6SPF =19HOLES 10,479' TO 10,482' WITH 6SPF =19HOLES 57HOLES TOTAL STAGE 8 TOOK 4,150PSI TO BREAK FORMATION AND SEAT BALL AT 10BPM FOLLOWED BY 3,500GALS OF 15% HCL ACID ONCE ACID ON MADE ADJUSTMENTS ON RATE TO GET MAIMUM BREAKS IN FORMATION THEN FOLLOWED FRAC SCHEDULE AS FOLLOWS: MA TREATING PSI=6,381PSI AVG TREATING PSI=4,434PSI ISIP=2,566PSI 5 MIN=2,553PSI MA INJECTION RATE=81.6BPM AVG INJECTION RATE=77BPM 10 MIN=2,534PSI 15 MIN=2,465PSI TOTAL FLUID INJECTED=267,033GALS TOTAL SAND INJECTED=312,715LBS RAN IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET PLUG @10,235' PERFS AS FOLLOW: 9,979' TO 9,982' WITH 6SPF =19HOLES 10,079' TO 10,082 WITH 6SPF=19HOLES 10,170' TO 10,182' WITH 6SPF=19HOLES 57 HOLES TOTAL NET PAGE; BWTR 46100 BWR BWUL 46100 Daily Cost $1,040.00 Cum Completion Cost: $52,340.00

11 UNIVERSITY 42-21 1 H 11-813 4.27.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 12340' 12050' 11760' 11450 11150 10530' 10235' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 12495' 10830 10830 10879' to 11102' COMENTS: WHEN SETTING PLUG DID NOT LOOK LIKE PLUG SET SO CAME OUT OF HOLE SLOW STAGE 9 PLUG WAS SET WENT BACK IN AND TAGGED PLUG AND SHOT PERFS TOOK 3.890PSI TO BREAK FORMATION AT 10BPM WITH 3,500GALS OF 15%HCL ACID BEHIND THE BALL CAME UP ON RATE AS FORMATION BROKE BACK TO THE SCHEDULE AS FOLLOWS: MA TREATING PSI=6,229PSI AVG TREATING PSI=4,294PSI MA INJECTION RATE=82BPM AVG INJECTION RATE=77BPM TOTAL FLUID INJECTED=209,030GALS ISIP = 2511 PSI 5 MIN = 2550 PSI 10 MIN = 2545 PSI 15 MIN = 2540 PSI COMENTS: WHEN ON 4# SAND PRESSURE WAS INCREASING SO WE CUT SAND EARLY FOR DESIGN SHUT DOWN FOR 4HRS FOR BREAK TO START STAGE 10 WIRE LINE PERFORATING WAS DELAYED DUE TO WIND,HALIBURTON WORKED ON PUMPS WAITING ON REPORT FORM THEM ABOUT HP FRAC WOULD BE DELAYED TILL THE AM BWTR 51077 BWR BWUL 51077 Daily Cost $1,040.00 Cum Completion Cost: $52,340.00

12 UNIVERSITY 42-21 1 H 11-813 4.28.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 12495' 10830 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9382' 10879' to 11102' WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET FRAC PLUG @9,930' SHOT PERFS AS FOLLOWS:9,670' TO 9,682' WITH 6SPF 19HOLES AVG PUMP DOWN PSI=2570 9,779' TO 9,782' WITH 6SPF 19HOLES AVG PUMP DOWN RATE=13BPM 9,879' TO 9,882' WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 10 TOOK 3,480PSI @ 10BPM TO SEAT BALL AND BREAK FORMATION WITH 3,500GALS OF 15% HCL ACID BEHIND BALL CAME UP ON RATE AS FORMATION GAVE IN THEN FOLLOWED FRAC SHEDULE AS FOLLOWS: MA TREATING PSI=6,354PSI AVG TREATING PSI=4,463PSI MA INJECTION RATE=79BPM AVG INJECTION RATE=77BPM TOTAL FLUID INJECTED=220,330GALS TOTAL SAND INJECTED=309,417LBS COMENTS:CUT SAND ON 4# NOT RUNNING THE DESIGN DUE TO PSI ISIP=2,550PSI 5 MIN=2,489PSI 10 MIN=2,478PSI 15 MIN=2,352PSI WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET FRAC PLUG @9,630' SHOT PERFS AS FOLLOWS:9,379' TO 9,382' WITH 6SPF 19HOLES AVG PUMP DOWN PSI=2475PSI 9,479' TO 9,482' WITH 6SPF 19HOLES AVG PUMP DOWN RATE=13BPM 9,579' TO 9,582' WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 11 TOOK 4,350PSI @ 10BPM TO SEAT BALL AND BREAK FORMATION WITH 3,500GALS OF 15% HCL ACID BEHIND BALL CAME UP ON RATE AS FORMATION GAVE IN THEN FOLLOWED FRAC SHEDULE AS FOLLOWS: MA TREATING PSI=6,154PSI AVG TREATING PSI=4,392PSI MA INJECTION RATE=80BPM AVG INJECTION RATE=77BPM CONT NET PAGE BWTR 56323 BWR BWUL 56323 Daily Cost $1,040.00 Cum Completion Cost: $53,380.00

13 UNIVERSITY 42-21 1 H 11-813 4.29.11 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 12495' 10830 8950' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 10879' to 11102' 8989' to 9192' HAD TO SHUT DOWN DUE TO THE WIND. BWTR 66553 BWR BWUL 66553 Daily Cost $0.00 Cum Completion Cost: $53,380.00

14 UNIVERSITY 42-21 1 H 11-813 4/30/2011 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 12495' 10830 8950' 10879' to 11102' 8989' to 9192' WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET FRAC PLUG @8,650' SHOT PERFS AS FOLLOWS:8,389' TO 8,392' WITH 6SPF 19HOLES AVG PUMP DOWN PSI=2,615PSI 8,489' TO 8492' WITH 6SPF 19HOLES AVG PUMP DOWN RATE=13BPM 8,589 TO 8,592 WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 14 TOOK 3,430PSI @ 10BPM TO SEAT BALL AND BREAK FORMATION WITH 3,500GALS OF 15% HCL ACID BEHIND BALL CAME UP ON RATE AS FORMATION GAVE IN THEN FOLLOWED FRAC SHEDULE AS FOLLOWS: MA TREATING PSI=5,336PSI AVG TREATING PSI=3,940PSI MA INJECTION RATE=79BPM AVG INJECTION RATE=76BPM TOTAL FLUID INJECTED=237,875GALS TOTAL SAND INJECTED=313,081LBS COMENTS: WHEN WE STARTED ON PAD WE COULD NOT MOVE GEL SHUT DOWN TO FI ISIP=2,468PSI 5 MIN=2,443PSI 10 MIN=2,410PSI 15 MIN=2,352PSI WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET FRAC PLUG @8,350'' SHOT PERFS AS FOLLOWS:8,089' TO 8,092' WITH 6SPF 19HOLES AVG PUMP DOWN PSI=2480PSI 8,189' TO 8,192' WITH 6SPF 19HOLES AVG PUMP DOWN RATE=13BPM 8,289' TO 8,292' WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 15 TOOK 3,945PSI @ 10BPM TO SEAT BALL AND BREAK FORMATION WITH 3,500GALS OF 15% HCL ACID BEHIND BALL CAME UP ON RATE AS FORMATION GAVE IN THEN FOLLOWED FRAC SHEDULE AS FOLLOWS: MA TREATING PSI=5,260PSI AVG TREATING PSI=4,031PSI MA INJECTION RATE=78BPM AVG INJECTION RATE=77BPM CONT NET PAGE BWTR 72217 BWR BWUL 72217 Daily Cost $4,361,187.00 Cum Completion Cost: $4,414,567.00

14 UNIVERSITY 42-21 1 H 11-813 4/30/2011 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' 8050' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 12495' 10830 8950' 10879' to 11102' 8989' to 9192' CONT 15 TOTAL SAND INJECTED=314,713LBS TOTAL FLUID INJECTED=206,268GALS ISIP=2,466PSI 5 MIN=2,488PSI 10 MIN=2,462PSI 15 MIN=2,431PSI COMENTS:STAGE WENT VERY WELL FOLLOWED FRAC SCHEDULE GOOD FLUSH WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET PLUG @8,050' PUMP DOWN AVG PSI=2,480PSI PUMP DOWN AVG RATE=13.2BPM SHOT PERFS AS FOLLOWS: 7,789'' TO 7,792'' WITH 6SPF 19HOLES 7,869' TO 7,872'' WITH 6SPF 19HOLES 7,985' TO 7,992' WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 16 TOOK 3250PSI TO BREAK FORMATION AND SEAT BALL AT 10BPM CHASING BALL WITH 3,500GALS OF 15%HCL ACID ONCE ACID ON FORMATION MADE RATE CHANGES AS FORMATION BROKE THEN FOLLOWED FRAC SCHEDULE AS FOLLOWS:MA INJECTION RATE 78BPM AVG INJECTION RATE=77BPM MA TREATING PSI=5,399PSI AVG TREATING PSI=4,182PSI TOTAL SAND INJECTED=315,495LBS TOTAL FLUID INJECTED=205,774GALS ISIP=2,671PSI 5 MIN=2,593PSI 10 MIN=2,491PSI 15 MIN=2,482PSI COMENTS:BEFORE THE STAGE THE FRAC VAN SHUT DOWN ON US WITH OUT STARTING ANYTHING THEY CHECKED OUT THE COMPUTER SYSTEM AND WENT AHEAD AND PUMPED JOB CONT NET PAGE BWTR 82028 BWR BWUL 82028 Daily Cost $4,361,187.00 Cum Completion Cost: $4,414,567.00

14 UNIVERSITY 42-21 1 H 11-813 4/30/2011 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' 8050' 7730' 7430' 12495' 10830 8950' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 10879' to 11102' 8989' to 9192' 7189' to 7392' WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET PLUG @7,730'' PUMP DOWN AVG PSI=2,585PSI PUMP DOWN AVG RATE=13.2BPM SHOT PERFS AS FOLLOWS:7,489' TO 7,492' WITH 6SPF 19HOLES 7,589' TO 7,592' WITH 6SPF 19HOLES 7,689' TO 7,692' WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 17 TOOK 3,780PSI TO BREAK FORMATION AND SEAT BALL CHASING BALL WITH 3,500GALS OF 15% HCL ACID AT 10BPM MAKING RATE ADJUSTMENTS AS ACID GETS ON FORMATION THEN FOLLOW FRAC SCHEDULE AS FOLLOWS: MA TREATING PSI=5,243PSI AVG TREATING PSI=4,015PSI MA INJECTION RATE=82BPM AVG INJECTION RATE=80BPM TOTAL FLUID INJECTED=211,873GALS TOTAL SAND INJECTED=310,146LBS ISIP=2,465PSI 5 MIN=2,444PSI 10 MIN=2,375PSI 15 MIN=2,320PSI COMENTS:WE LOST THE HOPPER TWO TIMES IN 3# SAND WE THE GOT THE HOPPER BACK AND WE KNEW THAT WE COULD GET BACK INTO FORMATION DECIDED TO RAMP OUR SAND SINCE SAND CONS. WAS SO LOW WE RAMPED SAND FROM A 2.6 TO GET TO A 4# SYSTEM WORKED WELL GOT OUR FORMATION TO TAKE OUR PLANED SAND VOLUME OF 4# SAND WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET PLUG @7,430'' PUMP DOWN AVG PSI=2,628PSI PUMP DOWN AVG RATE=13.2BPM SHOT PERFS AS FOLLOWS:7,189' TO 7,192' WITH 6SPF 19HOLES 7,289' TO 7,292' WITH 6SPF 19HOLE 7,389' TO 7,392' WITH 6SPF 19HOLES:57HOLES TOTAL BWTR 87073 BWR BWUL 87073 Daily Cost $4,361,187.00 Cum Completion Cost: $4,414,567.00

14 UNIVERSITY 42-21 1 H 11-813 4/30/2011 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' 8050' 7730' 7430' 12495' 10830 8950' 7130' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 10879' to 11102' 8989' to 9192' 7189' to 7392' STAGE 18 TOOK 3,290PSI TO BREAK FORMATION AND SEAT BALL AT 10BPM CHASING BALL WITH 3,500GALS OF 15%HCL ACID ONCE ACID ON FORMATION MADE RATE CHANGES AS FORMATION BROKE THEN FOLLOWED FRAC SCHEDULE AS FOLLOWS:MA INJECTION RATE 81BPM AVG INJECTION RATE=79BPM MA TREATING PSI=5,276PSI AVG TREATING PSI=3,965PSI TOTAL SAND INJECTED=297,531LBS TOTAL FLUID INJECTED=199,317GALS ISIP=2,691PSI 5 MIN=2,575PSI 10 MIN=2,533PSI 15 MIN=2,503PSI COMENTS:WE MADE A FEW ADJUSTMENTS WITH THE SAND CONVEYER STOPPING AND STARTING WHEN SAND CONC. WENT DOWN ON OTTAWA SAND WE STEPPED UP TO 4# TO MAKE IT BACK UP AND STAYED OF 4# LONGER THAN SCHEDULE TO MAKE UP THE SAND IN FORMATION WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL AND SET PLUG @ 7,130' PUMP DOWN RATE=13BPM PUMP DOWN AVG PSI= 2,620PSI SHOT PERFS AS FOLLOWS:6,889' TO 6,892' WITH 6SPF 19HOLES 6,989' TO 6,992 WITH 6 SPF 19HOLES 7,089' TO 7,092' WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 19 TOOK 3,345PSI TO BREAK FORMATION AND SEAT BALL AT 10BPM CHASING BALL WITH 3,500GALS OF 15%HCL ACID ONCE ACID ON FORMATION MADE RATE CHANGES AS FORMATION BROKE THEN FOLLOWED FRAC SCHEDULE AS FOLLOWS:MA INJECTION RATE 77BPM AVG INJECTION RATE=77BPM MA TREATING PSI=5,259PSI AVG TREATING PSI=3,777PSI TOTAL SAND INJECTED=318,087LBS TOTAL FLUID INJECTED=198,812GALS ISIP=2,696PSI 5 MIN=2,530PSI 10 MIN=2,503PSI 15 MIN=2,474PSI BWTR 96552 BWR BWUL 96552 Daily Cost $4,361,187.00 Cum Completion Cost: $4,414,567.00

14 UNIVERSITY 42-21 1 H 11-813 4/30/2011 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' 8050' 7730' 7430' 12495' 10830 8950' 7130' 6828' 6530' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 6589' to 6792' 6285' to 6492' 10879' to 11102' 8989' to 9192' 7189' to 7392' WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL SET PLUG @6,828' PUMP DOWN AVG PSI=2,609PSI PUMP DOWN AVG RATE=13.2BPM SHOT PERFS AS FOLLOWS:6,589' TO 6,592' WITH 6SPF 19HOLES 6,689' TO 6,692' WITH 6SPF 19HOLES 6,789' TO 6,792' WITH 6SPF 19HOLES 57HOLES TOTAL STAGE 20 TOOK 3,896PSI TO BREAK FORMATION AND SEAT BALL CHASING BALL WITH 3,500GALS OF 15% HCL ACID AT 10BPM MAKING RATE ADJUSTMENTS AS ACID GETS ON FORMATION THEN FOLLOW FRAC SCHEDULE AS FOLLOWS: MA TREATING PSI=5,034PSI AVG TREATING PSI=3,825PSI MA INJECTION RATE=78.6BPM AVG INJECTION RATE=76.8BPM TOTAL FLUID INJECTED=201,619GALS TOTAL SAND INJECTED=314,673LBS ISIP=2,737PSI 5 MIN=2,605PSI 10 MIN=2,528PSI 15 MIN=2,480PSI WENT IN HOLE WITH GUNS AND FRAC PLUG AND CCL AND SET PLUG @6,530' PUMP DOWN AVG PSI=2,580PSI PUMP DOWN AVG RATE=13.2BPM SHOT PERFS AS FOLLOWS:6,285' TO 6,292' WITH 6SPF 19HOLES 6,389' TO 6,392' WITH 6SPF 19HOLES 6,489' TO 6,492' WITH 6SPF 19HOLES 57HOLE TOTAL STAGE 21 TOOK 3,646PSI TO BREAK FORMATION AND SEAT BALL CHASING BALL WITH 3,500GALS OF 15% HCL ACID AT 10BPM MAKING RATE ADJUSTMENTS AS ACID GETS ON FORMATION THEN FOLLOW FRAC SCHEDULE AS FOLLOWS: MA TREATING PSI=5,034PSI AVG TREATING PSI=0PSI MA INJECTION RATE=78.6BPM AVG INJECTION RATE=77BPM BWTR 101352 BWR BWUL 101352 Daily Cost $4,361,187.00 Cum Completion Cost: $4,414,567.00

14 UNIVERSITY 42-21 1 H 11-813 4/30/2011 12744' PERF - FRAC 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' 8050' 7730' 7430' 12495' 10830 8950' 7130' 6828' 6530' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 6589' to 6792' 6285' to 6492' 10879' to 11102' 8989' to 9192' 7189' to 7392' STAGE 21 TOTAL SAND INJECTED=275,311LBS TOTAL FLUID INJECTED=195,313GALS CON ISIP=2,628PSI 5 MIN=2,371PSI 10 MIN= 2.301PSI 15 MIN=2,242PSI COMENTS: STILL WAITING FOR TICKET AND FINAL TREATMENT REPORT ON STAGE 21 TOTAL FLUID TO RECOVER =108,758BBLS FLOWING WELL BACK : SOUTHWEST WELL TENDING REPORT TIME: 6:00 AM 5/1/11 DOWN SALES LINE: N TBG PSI: 0 CSG PSI: 1820 RATE: 72 BWPH 0 BOPH Co2: 0 CHOKE: 14/64 FLUID RECOVERED LAST 24 HRS: 81 BW 0 BO TOTAL FLUID RECOVERED: 81 BW 0 BO TOTAL SAND INJECTED: 6409196 100 MESH = 443161 OTTAWA 20/40 = 2646575 SUPER LC 20/40 = 1985835 WHITE 20/40 = 1333625 BWTR 108758 BWR 81 BWUL 108677 Daily Cost $4,361,187.00 Cum Completion Cost: $4,414,567.00

15 UNIVERSITY 42-21 1 H 11-813 5.1.11 12744' FLOW BACK 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' 8050' 7730' 7430' 12495' 10830 8950' 7130' 6828' 6530' 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 6589' to 6792' 6285' to 6492' 10879' to 11102' 8989' to 9192' 7189' to 7392' FLOWING WELL BACK : SOUTHWEST WELL TENDING REPORT TIME: 6:00 AM 5/2/11 DOWN SALES LINE: N TBG PSI: 0 CSG PSI: 1200 RATE: 74 BWPH 0 BOPH Co2: 0 CHOKE: 16/64 FLUID RECOVERED LAST 24 HRS: 1805 BW 0 BO TOTAL FLUID RECOVERED: 1886 BW 0 BO BWTR 108758 BWR 1886 BWUL 106872 Daily Cost $1,000.00 Cum Completion Cost: $4,415,567.00

16 UNIVERSITY 42-21 1 H 11-813 5.2.11 12744' DRILL PLUGS 22 5 1/2" 17# N 80 12744.42 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' Drilled 8050' Drilled 7730' Drilled 7430' Drilled 10830 8950' 7130' Drilled 6828' Drilled 6530' Drilled 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 6589' to 6792' 6285' to 6492' 10879' to 11102' 8989' to 9192' 7189' to 7392' MOVE IN HALLIBURTON COIL TUBING UNIT AND RIGG THEM UP AND ATTEND SAFETY MEETING STARTED IN HOLE WITH COIL BROKE CIRCULATION STARTED IN AFTER FIRST PLUG TAGGED FIRST PLUG @6,505' WITH A CIRCULATE PSI OF 2,722PSI AND A RATE OF 2BBLS IN AND 4BBLS OUT DRILLED THREW PLUG WITH WELL HEAD PSI 801 THEN RAN A GEL SWEEP HEADING TO NET PLUG TAGGED PLUG @6,803' WITH A CIRCULATE PSI OF 3,384PSI AND A RATE OF 2BBLS IN AND 4BBLS OUT DRILLED THREW PLUG WITH WELL HEAD PSI 840 THEN RAN A GEL SWEEP HEADING TO NET PLUG TAGGED NET PLUG @7,107' THEN SHORT TRIPPED TO 5,200' AND WENT BACK IN HOLE TO 7,107 AND 4BBLS OUT WITH A WELLHEAD PSI OF 690 TAGGED PLUG @ 7,407' WITH A CIRCULATE PSI OF 4,100 AND A RATE OF 2.5BLS IN AND 4 BBLS OUT DRILLED THREW PLUG WITH WELL HEAD PSI 767 THEN RAN GEL SWEEP HEADING TO NET PLUG TAGGED NET PLUG @7,706' THEN SHORT TRIPPED TO 5,200' AND WENT BACK IN HOLE TO 7,706' DRILLED THREW PLUG WITH 4,670 CIRCULATING PSI AND A RATE OF 2BBLS IN AND 3BBLS OUT WITH A WELL HEAD PSI 792 THEN RAN GEL SWEEP AND CLEANED OUT CHOKE DROPPING OUR CIRCULATING PSI TO 3,860 AND WELL HEAD TO 700 PSI AND HEADED TO NET PLUG TAGGED PLUG @ 8,029' WITH A CIRCULATE PSI OF 3,465 AND A RATE OF 2BLS IN AND 4 BBLS OUT WITH A WELL HEAD PSI 678 THEN RAN GEL SWEEP HEADING TO NET PLUG BWTR 108758 BWR 1886 BWUL 106872 Daily Cost $1,000.00 Cum Completion Cost: $4,415,567.00

16 UNIVERSITY 42-21 1 H 11-813 5.2.11 12744' DRILL PLUGS 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10,235 9930' 9630' 9250' 8650' 8350' Drilled 8050' Drilled 7730' Drilled 7430' Drilled 12495' 10830 8950' 7130' Drilled 6828' Drilled 6530' Drilled 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 6589' to 6792' 6285' to 6492' 10879' to 11102' 8989' to 9192' 7189' to 7392' TAGGED PLUG @8,330' THEN SHORT TRIPPED TO 5200' RAN BACK IN HOLE TO 8,330' END OF REPORT FOR THE DAY FLOWING WELL BACK : SOUTHWEST WELL TENDING REPORT TIME: 6:00 AM 5/3/11 DOWN SALES LINE: N TBG PSI: 0 CSG PSI: 640 RATE: 101 BWPH 123 BWIPH Co2: 0 CHOKE: 45/64 FLUID RECOVERED LAST 24 HRS: 2238 BW 2147 BW INJECTED TOTAL FLUID RECOVERED: 4168 BW 2147 BW INJECTED BWTR 108758 BWR 4168 BWUL 104590 Daily Cost $1,000.00 Cum Completion Cost: $4,415,567.00

17 UNIVERSITY 42-21 1 H 11-813 5.3.11 12744' DRILL PLUGS 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10235 Drilled 9930' Drilled 9630' Drilled 9250' Drilled 8650' Drilled 8350' Drilled 8050' Drilled 7730' Drilled 7430' Drilled 12495' 10830 8950' Drilled 7130' Drilled 6828' Drilled 6530' Drilled 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 6589' to 6792' 6285' to 6492' 10879' to 11102' 8989' to 9192' 7189' to 7392' WENT BACK IN HOLE WITH NEW BIT ON SHORT TRIP TAGGED @8,330' DRILLED PLUG WITH A CIRCULATING PSI OF 2,180 AND A RATE OF 2.5BBLS IN AND 3.5 OUT AND A WELL HEAD PSI OF 582 THREW PLUG THEN RAN A GEL SWEEP HEADING TO NET PLUG TAGGED PLUG @8,689' PLUG WAS SUPPOSE TO BE @8,650' DETERMINED THAT WE WERE PUSHING NUMBER SEVEN PLUG DOWN TO IT DRILL THREW IT WITH A CIRCULATING PSI OF 3,100 AND A RATE OF 2BBLS IN AND 3BBLS OUT AND WELL HEAD PSI OF 623 THEN RAN A GEL SWEEP HEADING TO NET PLUG TAGGED NET PLUG @8,939' DRILLED THREW IT WITH A CIRCULATING PSI OF 2,600 AND A RATE OF 2.5BBLS IN AND 3.5BBLS OUT AND WELL HEAD PSI OF 624 THEN RAN GEL SWEEP HEAD TAGGED PLUG @9,238' THEN CAME OUT FOR A SHORT TRIP THEN BACK IN HOLE TO 9,238' DRILLED THREW PLUG WITH A CIRCULATING PSI OF 2,764 AND A RATE OF 2BBLS IN AND 3.5BBLS OUT AND A WELL HEAD PSI OF 581 AND THEN RAN A GEL SWEEP TAGGED PLUG @ 9,630' WITH A CIRCULATE PSI OF 2,914 AND A RATE OF 2BLS IN AND 4 BBLS OUT AND A WELL HEAD PSI OF 606 AND THEN RAN A GEL SWEEP HEADING TO NET PLUG TAGGED PLUG @9,930' THEN CAME OUT FOR A SHORT TRIP THEN BACK IN HOLE TO 9,930' DRILLED THREW PLUG WITH A CIRCULATING PSI OF 2,560 AND A RATE OF 2BBLS IN AND 3BBLS OUT AND A WELL HEAD PSI OF 573 THEN RAN A GEL SWEEP HEADING TO NET PLUG TAGGED PLUG @10,227' WITH A CIRCULATING PSI OF 2,800 AND A RATE OF 2BBLS IN AND BWTR 108758 BWR 6429 BWUL 102329 Daily Cost $1,000.00 Cum Completion Cost: $4,415,567.00

17 UNIVERSITY 42-21 1 H 11-813 5.3.11 12744' DRILL PLUGS 22 5 1/2" 17# N 80 12744.42 2 3/8" 4.7# N-80 400 12340' 12050' 11760' 11450 11150 10530 10235 Drilled 9930' Drilled 9630' Drilled 9250' Drilled 8650' Drilled 8350' Drilled 8050' Drilled 7730' Drilled 7430' Drilled 12495' 10830 8950' Drilled 7130' Drilled 6828' Drilled 6530' Drilled 12499' to 12402' 12099' to 12302' 11799' to 12002' 11499' to 11702' 11199' to 11402' 10579' to 10782' 10279' to 10483' 9979' to 10182' 9670' to 9882' 9379' to 9582' 8689' to 8892' 8389' to 8592' 8089' to 8292' 7789' to 7992 7489' to 7692' 6889' to 7092' 6589' to 6792' 6285' to 6492' 10879' to 11102' 8989' to 9192' 7189' to 7392' 4BBLS OUT WITH A WELL HEAD PSI OF 585 THEN RAN A GEL SWEEP HEADING TO NET PLUG TAGGED PLUG @10,520' THEN CAME OUT OF HOLE FOR SHORT TRIP END OF REPORT FOR DAY FLOWING WELL BACK : SOUTHWEST WELL TENDING REPORT TIME: 6:00 AM 5/4/11 DOWN SALES LINE: N TBG PSI: 0 CSG PSI: 420 RATE: 170 BWPH 149 BWIPH Co2: 0 CHOKE: 41/64 FLUID RECOVERED LAST 24 HRS: 2305 BW 3005 BW INJECTED NET RECOVERED 5310 TOTAL FLUID RECOVERED: 6429 BW 5152 BW INJECTED NET RECOVERED 11581 BWTR 108758 BWR 6429 BWUL 102329 Daily Cost $1,000.00 Cum Completion Cost: $4,415,567.00