West. PS (PowerSouth Energy Cooperative) SMEPA (South Mississippi Electric Power Association) Southern Company Transmission

Similar documents
West. PS (PowerSouth Energy Cooperative) SMEPA (South Mississippi Electric Power Association) Southern Company Transmission

West. Coordinated Planning. PS (PowerSouth Energy Cooperative) SMEPA (South Mississippi Electric Power Association) Southern Company Transmission

West. Coordinated Planning. Coordinated Planning. PS (PowerSouth Energy Cooperative) SMEPA (South Mississippi Electric Power Association)

East. Dalton Utilities. GTC (Georgia Transmission Corporation) MEAG (Municipal Electric Authority of GA) Southern Company Transmission

2011 SERTP Annual l S E S RTP T P S u S mmit 1

Southeastern Region Transmission Planning. 10 Year Transmission Expansion Plan

East. Dalton Utilities. GTC (Georgia Transmission Corporation) MEAG (Municipal Electric Authority of GA) Southern Company Transmission

1st Division Commander Tina Bush (256)

East. Georgia Integrated Transmission System (ITS) Jointly Planned ITS. Dalton Utilities. GTC (Georgia Transmission Corporation)

Southeastern Regional Transmission Planning Process 10 Year Preliminary Expansion Plan Meeting. June 24, 2009

Transmission Improvements Plan for 575 MW Network Service Request Wansley CC 7 Generation Facility (OASIS # ) Georgia Transmission Corporation

East. Georgia Integrated Transmission System (ITS) GTC (Georgia Transmission Corporation) MEAG (Municipal Electric Authority of GA)

ALABAMA ASSET QUALITY - JUNE 30, 2017

2010 SERTP. Welcome. SERTP rd Quarter Meeting. 2 nd RPSG Meeting 9:00 AM 3:00 PM

Southern Company Transmission Active OATT Interconnection Agreements

Entergy Gulf States, Inc. (Texas) Proposed Transmission Reliability Projects

SERTP rd Quarter Meeting

Twin Cities Minnesota Zone Meeting Xcel Energy. May 11, 2005 Bloomington, MN

Entergy Texas, Inc. Transmission Draft Construction Plan Update 1 Projects

SERTP rd Quarter Meeting

Falcon-Midway 115 kv Line Uprate Project Report

Southeastern Regional Transmission Planning (SERTP) PRELIMINARY 10 YEAR TRANSMISSION EXPANSION PLANS

Southeastern Regional Transmission Planning (SERTP) PRELIMINARY 10 YEAR TRANSMISSION EXPANSION PLANS

SERTP nd Quarter Meeting

Status of PNM s Completed Transmission Construction Projects 11/30/2017

2013 SERTP. Welcome. SERTP rd Quarter Meeting. 2 nd RPSG Meeting

Large Load Serving Study Report for La Plata Electric Association, Inc. Alternatives. Addendum. San Juan Major Project

VACAR 2015 SUMMER PEAK RELIABILITY STUDY

MTEP13 SPM #2- Central Region. March 25, 2013

South Dakota 890 Study

Sub Regional RTEP Committee Mid-Atlantic First Energy MAAC Solution Meeting

THE NECESSITY OF THE 500 KV SYSTEM IN NWE S TRANSMISSION SYSTEM TO MAINTAIN RELIABLE SERVICE TO MONTANA CUSTOMERS

Sub Regional RTEP Committee Mid-Atlantic

South Carolina Electric and Gas Company Planned Transmission Projects $2M and above Total 5 Year Budget

Transmission Expansion Advisory Committee

SPP Notification to Construct

Elbert County 500 MW Generation Addition Interconnection Feasibility Study Report OASIS POSTING # GI

Chapter 7 - Appendix A

Sub Regional RTEP Committee - Southern. August 19, 2011

Outer Metro 115 kv Transmission Development Study. (Scott Co, Carver Co and Hennepin Co)

ATTACHMENT B - Table 1: LIST OF MANAGEMENT-APPROVED PROJECTS UNDER $50M

Emera Maine Representative: Jeffrey Fenn, P.E., SGC Engineering LLC

Entergy Louisiana, LLC (South) & Entergy New Orleans, Inc. Proposed Transmission Reliability Projects

National Grid s 2017 Local Transmission Plan

Sub-Regional RTEP Committee PJM South

Tri-State December 2013 Board Meeting

OCTOBER 17, Emera Maine Representative: Jeffrey Fenn, P.E., LR/SGC Engineering LLC

National Grid s 2018 Local Transmission Plan

Generation Interconnection Impact Study Results for Eurus Energy America Corporation s Eurus Combine Hills I, LLC Power Project.

South Carolina Electric and Gas Company Planned Transmission Projects $2M and above Total 5 Year Budget

APPENDIX E: Project Need and Description

PJM SRTEP Meeting Questions Pertaining to Proposed Projects & Scopes AEP: Ambler Ridge:

Published by Roundabout Publications PO Box Lenexa, KS Phone Internet

Project #148. Generation Interconnection System Impact Study Report

Appendix B. Summary of Changes to the Year Assessment

First Energy Generator Deactivation Request - January Deactivation Study Results and Required Upgrades April 25, 2012

APPENDIX E: Project Need and Description

South Carolina Regional Transmission Planning. Stakeholder Meeting. Web Conference

Sub Regional RTEP Committee Mid-Atlantic

Key to Status Fields in the Project List

APPENDIX F: Project Need and Description

Appendix D Black Hills Project Summary

Black Hills Project Summary

Western Area Power Administration Rocky Mountain Region Annual Progress Report. Projects. Weld Substation Stage 04

Generation Deactivation Notification Update

2016 SPP Transmission Expansion Plan Project List Kansas Projects

100 MW Wind Generation Project

Emera Maine Representative: Jeffrey Fenn, P.E., SGC Engineering LLC

Feasibility Study Report

Illinois State Report

Designated Network Loads and Resources Load Served by Company Owned Resources

PG&E s 2012 Request Window Proposals

Taylors Ferry on Bankhead Lake Off the Grid Cabins

SPP Notification to Construct

Impacts of MISO DPP-2016-February (West, ATC, MI, South) Projects on PJM Facilities

South Carolina Electric and Gas Company Planned Transmission Projects $2M and above Total 5 Year Budget

March 18, Subject: Imperial Irrigation District 2014 Annual Progress Report - Rev 1

Proposed New Construction for

SPP Notification to Construct

Pacific Gas and Electric Company s Revised 2015 Annual Progress

ATC Year Assessment Network Project List. MTEP Cost Reason for Change since Previous System Addition

TRANSMISSION PLANNING CRITERIA

Sub Regional RTEP Committee Western Region ATSI

Pacific Gas and Electric Company s Revised 2016 Annual Progress

Minnesota Biennial Transmission. Zone Meeting 8

Sub Regional RTEP Committee Mid-Atlantic

Transmission Planning. WECC 2014 Progress Report. March 14, 2014

2013 ANNUAL PROGRESS REPORT

Q0044 interconnection at

KEY. Key to Status Fields in the Project List

Review Initial Results of Reliability Assessments. Inter-regional. Discuss Alternative Solutions from Stakeholders

Key to Status Fields in the Project List KEY

Local Transmission Plan. October 11, 2013 Revised August 25, 2014

APPENDIX F: 2012 Request Window Submittals

PJM Sub Regional RTEP Committee Mid-Atlantic January 22, Esam Khadr, Sr. Director Electric Delivery Planning, PSE&G

Generation Interconnection Feasibility Study For XXXXXXXXXXXXXXXXXXXXXX MW generator at new Western Refinary Substation

Sub Regional RTEP Committee Mid-Atlantic

Final System Impact Study for. Sierra Pacific Industries 31 MW Generation Project. Mount Vernon, WA. November 16, 2006

7.7 Southeast Zone. Transmission Projects Report Section 7: Needs

DFO STATEMENT OF NEED REPORT

Transcription:

West PS (PowerSouth Energy Cooperative) SMEPA (South Mississippi Electric Power Association) Southern Company Transmission

Expansion Item W-1 Anniston Area Improvement Reconductor 1.5 miles with 795 ACSR along the Anniston Oxanna 115 kv T.L. Create a new 115 kv T.L. from Anniston to Crooked Creek. 2014 The loss of the West End DS Oxanna Tap 115 kv line section, causes the southern end of the Anniston Crooked Creek 115 kv T.L. to become overloaded. Voltage Support.

Anniston Area Improvement To GADSDEN To HAMMOND N.O. To HENRY DAM ALEX XRDS WEAVER BONNIE BROOK Reconductor DIAGRAM 1.6 miles 4-E 2/0 Cu along Anniston Anniston Oxanna Area Reconfiguration Improvement 115 kv T.L. with 795 ACSR (1.) Reconductor 1.59 miles 2/0 Cu in the existing Anniston Oxanna 115 kv TL with 795 ACSR. Reconnect 0.67 miles of 397 ACSR (2.) Reconnect 0.67mi of 397 ACSR tap to Oxanna TS to the Anniston Bynum 115 kv TL (1351 ACSS) with a 3-way tap 115kV to switch Oxanna at the tap to point. the Anniston Bynum 115 kv T.L. (3.) Isolate the Anniston loop load from Crooked Creek by breaking the tie as shown in Diagram 3. (4.) Add a second 795 ACSR circuit to existing double circuit structures on the West End Greenbrier pole line and reconductor with 795 ACSR to complete the new Anniston Crooked Creek 115 kv TL. Add a second 795 ACSR circuit on the West End Greenbrier pole line and reconductor with 795 ACSR to (5.) Shift the N.O. section from Lenlock to Alexandria complete Crossroads the new Anniston Crooked Creek 115 kv T.L. CENTRAL CASTINGS ANNISTON FLATBRIDGE OXFORD CHEAHA WEST END OXANNA LENLOCK CPL OXFORD FRIENDSHIP N. QUINTARD FT. MCCELLAN HENRY RD GREENBRIER GOLDEN SPRINGS To CROOKED CREEK

Expansion Item W-2 Marianna Highland City 115 kv T.L. Reconductor 47.8 miles of 115 kv T.L. from Marianna to Highland City with 1033 ACSR at 100 C. 2015 The loss of Holmes Creek Highland City 230 kv T.L., with Smith Unit #3 offline, causes the Marianna Highland City 115 kv T.L. to become overloaded.

PLANT FARLEY PINCKARD OPP Marianna Highland City 115 kv T.L. WEBB COTTONWOOD SAMSON GENEVA PITTMAN HOLMES CREEK MARIANNA PLANT SHOAL RIVER ALFORD SI Reconductor Marianna Alford Tap 115 kv TL Reconductor Alford Tap Highland City 115 kv TL SANTA ROSA PLANT SMITH LAGUNA BEACH HIGHLAND CITY CALLAWAY

Expansion Item W-3 Santa Rosa Laguna Beach 230 kv T.L. Construct a new Santa Rosa 230 kv substation with one 230 / 115 kv transformer. Replace Laguna Beach Santa Rosa #1 115 kv T.L. with a new 230 kv T.L (1351 ACSR). 2015 Several transmission lines in the Fort Walton Beach area exceed their thermal ratings under contingency conditions.

Santa Rosa Laguna Beach 230 kv T.L. New Laguna Beach Santa Rosa 230 kv T.L. Replace existing Laguna Beach Santa Rosa 115 kv T.L. with a parallel 230 kv T.L. Laguna Beach Substation Santa Rosa Substation

Expansion Item W-4 Greene County Bassett Creek 230 kv T.L. Construct 58.0 miles of new 230 kv T.L. from Greene County to Bassett Creek with 1351 ACSS at 200 C. Convert Bassett Creek 115 kv switching station to a 230 / 115 kv substation. 2015 The loss of Millers Ferry Camden Tap 115 kv T.L., with Crist offline, causes the Octagon Thomasville 115 kv T.L. to become overloaded.

Greene County Bassett Creek 230 kv T.L. PLANT GREENE COUNTY BELLAMY S.S. DEMOPOLIS SELMA B.W. BOGUE NAHEOLA S.S. OCTAGON S.S. R.F. HENRY DAM MILLERS FERRY DAM Convert Bassett Creek 115 kv switching station to a 230/115 kv substation LS Steel #2 THOMASVILLE T.S. THOMASVILLE TDS. LS Steel #1 FULTON GDC BASSETT CREEK PINE HILL KIMBROUGH CAMDEN INT. PAPER PINE HILL New Greene County Bassett Creek 230kV TL 58.0 miles of 1351.5 54/19 ACSS @ 200ºC, Rate B = 2277 A JACKSON BOISE PLANT LOWMAN

Expansion Item W-5 North Brewton Alligator Swamp 230 kv T.L. Construct approximately 56 miles of new 230 kv transmission line from North Brewton Alligator Swamp with 1351 ACSS at 200 C. 2015 The loss of one Chickasaw Silverhill 230 kv T.L., with Crist offline, causes the parallel Chickasaw Silverhill 230 kv T.L. and Barry Crist 230 kv T.L. to become overloaded.

North Brewton Alligator Swamp 230 kv T.L. NORTH BREWTON ELLICOTT PLANT BARRY Construct 56 miles of new 230 kv line from North Brewton to Alligator Swamp BIG CREEK CHICKASAW WADE PLANT DANIEL THEODORE MOSS POINT EAST SILVERHILL ELSANOR BELLVIEW PLANT CRIST BRENTWOOD

Expansion Item W-6 Enterprise Area Project Construct a new 230 / 115 kv substation, South Enterprise TS that taps the Pinckard Opp 230 kv T.L. Construct 6.0 miles of 115 kv transmission line from South Enterprise Enterprise with 795 ACSS at 160 C. 2015 The loss of the Pinckard Enterprise #1 115 kv T.L., with Smith Unit #3 offline, causes sections of the Pinckard Enterprise #2 115 kv T.L. to overload and vice versa.

Enterprise Area Project (5.) Westgate Rucker Blvd (2.) Ft. Rucker Newton (6.) Enterprise Daleville Pinckard (3.) S. Enterprise Dothan TS (1.) (4.) Enterprise Area Solution (1.) Upgrade approximately 2.33 mi of 266.8 26/7 ACSR 115 kv TL to 100 C (2013) (2.) Reconductor 0.31 mi of 397.5 ACSR with 795 26/7 ACSR (2014) (3.) Construct a new 230 / 115 kv substation (2015) (4.) Loop in the Opp (PS) Pinckard 230 kv TL into the new substation (2015) (5.) Construct a new 115 kv line terminal at Enterprise TS (2015) (6.) Construct approximately 5 mi of 795 ACSR 115 kv TL (2015)

Expansion Item W-7 Tuscaloosa Area Improvement Install a 230 / 115 kv transformer at a new substation, Moundville TS. Convert Moundville (to be called North Moundville DS) and Akron 44 kv substations to 115 kv Construct a new 115 kv T.L. from North Moundville to Moundville. Construct a new 115 kv T.L. from North Moundville to Big Sandy/Englewood Tap 2015 Overloads caused by multiple contingencies. Voltage Support.

Expansion Item W-8 Tuscaloosa Area Improvement Install a new 115 kv T.L. from Englewood to South Tuscaloosa Reconductor 3.6 miles of existing 115 kv T.L. from Big Sandy to Big Sandy Tap with 397 ACSR 2015 The loss of the Duncanville Bradley Rd 230 kv T.L., with Gorgas unit #10 offline, causes the Eutaw Moundville Tap 115 kv T.L. to become overloaded

Tuscaloosa Area Improvement PLANT GORGAS ALICEVILLE STANSEL BLACK WARRIOR LEWISTON EUTAW GORDO TO GORDO CARROLLS CREEK FAYETTE HWY HUNT OIL GOODRICH N MOUNDVILLE D.S. COLONIAL D.S. CPL MOUNDVILLE WESTERVELT AKRON D.S. LAKELAND YACHT CLUB TUSC. T.S. SONAT BANKHE AD EL PASO DAM HOLT T.S. J.W. #5 HOLT DAM BLACK WARRIOR EUTAW HWY SOUTH ROMULUS TUSC. T.S. STOKES BRADLEY ROAD ENGLEWOOD PPL AKRON NUCO R STEEL BIG SANDY MOUNDVILLE KELLERMAN JWR #4 TAYLORS FERRY SHOAL CREEK MERCEDES DUNCANVILLE S.S. New South Tuscaloosa Englewood 115 kv T.L. (2015) LAKEVIEW SOUTH BESSEMER T.S. BLOCTON New Moundville North Moundville 115 kv T.L. (2015) CPL EPES EPES T.S. LIVINGSTON MANNINGTON WOOD FLOORS BIRDEYE T.S. BIRDEYE D.S. PLANT GREENE COUNTY New Moundville 230 / 115 kv Substation (2015)

Expansion Item W-9 Barry Crist 230 kv T.L. Upgrade 31.6 miles along the Barry SP Crist SP 230 kv T.L. to 125 C operation. 2017 The loss of Barry S.P. Chickasaw 230 kv T.L., with Crist unit #7 offline, causes the Barry S.P. Crist S.P. 230 kv T.L. to exceed its thermal rating.

Barry Crist 230 kv T.L. Upgrade Barry Crist 230 kv T.L. to 125 degree C Operation from Alabama State Line to Plant Crist

Expansion Item W-10 Jasper Area Improvements Construct a new switching station, Jasper SS, near Jasper TS tap Loop in the Jasper TS Oakman and Jasper DS Taft Coal 161 kv transmission lines Reconductor 13.8 miles from Gorgas Jasper Tap 161 kv transmission line with 795 ACSR Reconductor 5.3 miles along the Jasper TS Parkland SS 161 kv with 795 ACSR. 2017 The loss of the Gorgas Scrubber #1 Gorgas 161 kv transmission line causes the Gorgas Taft Coal Jasper Tap 161 kv transmission line to become overloaded.

Jasper Area Improvements Reconductor 5.3 miles of existing 250MCM CU from Jasper TS Parkland Parkland SS 161 kv TL with 795 26/7 ACSR@ 100 C BANKSTON DS CHEVRON MINING (TYRO CREEK) Install New Jasper Switching Station, 5-Breaker Ring Bus Reconductor 13.8 miles of existing 250MCM CU from Gorgas Taft Coal to new Switching Station 161 kv TL with 795 26/7 ACSR@ 100 C N.O. BERRY DS CHEVRON MINING (FLAT CREEK) CHEVRON MINING (CEDAR CREEK) PROSPECT DS JASPER TS PARKLAND SS JASPER SS CURRY PARKLAND DS WALSTON RD JASPER DS GORGAS SCRUBBER #1 TAFT COAL BURROWS XRDS EAST JASPER Gorgas SP SMITH DAM Construct 0.8 mile 795 26/7 ACSR @ 100 C from tap point to Jasper TS parallel to existing 161kV TL To Miller Scrubber To Plant Miller NORTH SAMANTHA To Holt TS 230/115 kv #1 Auto To Holt TS 230/115 kv #2 Auto

Expansion Item W-11 Silverhill Turkey Hill 115 kv T.L. Construct approximately 2.75 miles of new 115 kv T.L. from Barnwell Tap Turkey Hill to complete the new Silverhill Turkey Hill 115 kv T.L. 2018 The loss of the Silverhill SW Foley 115 kv T.L., with Crist unit #7 offline, causes several sections from Silverhill to Turkey Hill to become overloaded.

Silverhill Turkey Hill 115 kv T.L. BELFOREST SILVERHILL FAIRHOPE PS - SILVERHILL POINT CLEAR FISH RIVER CAPACITOR C FISH RIVER BARNWELL B A MAGNOLIA RIVIERA UTIL. SW FOLEY FOLEY SS TURKEY HILL SS Construct 2.75 miles of new 115 kv T.L. from Barnwell Tap Turkey Hill SS

Expansion Item W-12 Barry Chickasaw 230 kv T.L. Reconductor 18.6 miles of 230 kv T.L. from Barry Steam Plant Chickasaw T.S. with 2-795 ACSS at 200 C. 2021 The loss of the Barry Crist 230 kv T.L., with Crist unit #7 offline, causes the Barry Chickasaw 230 kv T.L. to become overloaded.

Barry Chickasaw 230 kv T.L. Reconductor the Barry Chickasaw 230 kv TL (18.6 miles)

Expansion Item W-13 West McIntosh Calvert #2 230 kv T.L. Construct 11.4 miles of new 230 kv T.L. from West McIntosh to Calvert with 1351 ACSS at 200 C. 2021 The loss of West McIntosh Calvert #1 230 kv T.L., with Crist offline, causes the Barry McIntosh A and Barry CAES 115 kv T.L.s to become overloaded.

West McIntosh Calvert #2 230 kv T.L. WEST MCINTOSH T.S. Construct a new parallel, West McIntosh Calvert S.S. 230kV TL C.A.E.S. OLIN CORP. MCINTOSH T.S. TATE & LYLE Loss of West McIntosh Calvert S.S. 230kV TL and Crist Offline Increased Loading A Increased Loading TENSAW S.S. MT. VERNON T.S. CALVERT S.S. FLORIDA GAS MT. VERNON D.S. ELLICOTT S.S. BUCKS S.S. BARRY S.P.

South Mississippi Electric Power Association

Expansion Item SME-1 South Hoy 161 KV Source 2015 Construct a new 161 / 69 KV substation at South Hoy. Construct a new 161 KV T.L. from Moselle to South Hoy. This project alleviates 69 KV low voltages and multiple line overloads during 69 KV contingencies.

South Hoy 161 KV Source

Expansion Item SME-2 Homewood Station Creek 161KV Line Construct a new 161KV line from Homewood Station Creek utilizing the existing 69KV lines built w/ double circuit specifications from Homewood Sylvarena Sylvarena GT Taylorsville Station Creek This project alleviates loading on the Homewood 161/69 KV auto transformers and alleviates multiple 69 KV line overloads during system contingencies. 2016

Homewood Station Creek 161 KV Line

Expansion Item SME-3 Northwest Perry 161 / 69 KV Substation Tap 161 KV Line 162 and 69 KV Line 114 Construct Northwest Perry 161 / 69 KV Substation This project alleviates 69 KV low voltages and multiple line overloads on the Moselle Hintonville 69 KV loop during certain contingencies and supports the high load growth area near Petal. 2016

Northwest Perry 161 / 69 KV Substation

Expansion Item SME-4 Plant Morrow to Purvis Bulk 161 KV Line Tap 161 KV Line 166 Construct new 161 KV line from Plant Morrow to Tap Point Uprate existing line section from Tap Point to Purvis Bulk This project alleviates line overloads for the contingency of parallel line s 169 or 170 (Plant Morrow Purvis Bulk 161kV). The outage of one line overloads the adjacent line. 2021

Plant Morrow Purvis Bulk 161 KV Line

Expansion Item SME-5 Lumberton Benndale 161 KV Conversion Rebuild the Wiggins Stillmore, Wiggins Big Level and Benndale Benndale GT line sections to 161 KV specifications Convert the Stillmore and Big Level distribution substations to 161 KV Convert the Lumberton Big Level loop to 161 KV operation This project alleviates 69 KV low voltages and line overloads in the Lumberton and Benndale areas during certain contingencies 2021

Plant Morrow Purvis Bulk 161 KV Line

PowerSouth

Expansion Item PS-1 Brewton/Atmore Area Upgrade 40 miles of 46kV transmission line to 115kV 795 ACSR. 2014 This area experiences line overloads under single contingencies and unacceptable low voltage under a double contingency scenario. Alleviate voltage and overload problems by providing a parallel 115kV path that eliminates the overload and assures that the voltage is supported for the loss of two sources.

Brewton / Atmore Area Upgrade 40 miles of 46kV line to 115kV, 795 ACSR

Expansion Item PS-2 McWilliams-Fuller 115kV Conversion Upgrade 30 miles of 46kV transmission line to 115kV 795 ACSR. 2015 Alleviate voltage and overload problems by providing a parallel north-south 115kV path that eliminates the overload and assures that the voltage is supported for the loss of two sources.

McWilliams-Fuller Upgrade 30 miles of 46kV line to 115kV, 795 ACSR

Expansion Item PS-3 Hayes-Bottoms Mill 115kV TL Build new 16 mile 115kV 795 ACSR transmission line. Alleviate voltage and overload problems by providing a parallel north-south 115kV path that eliminates the overload and assures that the voltage is supported for the loss of two sources. 2015

Hayes-Bottoms Mill Build 16 miles of 115kV, 795 ACSR transmission line

Expansion Item PS-4 Gaskin-Southport 115kV TL Build new 12 mile 115kV 795 ACSR transmission line. Provide looped service to 3 member substations to improve reliability in the area. Also to help support voltage for certain N-2 contingencies. 2016

Gaskin-Southport Build 12 miles of 115kV, 795 ACSR transmission line

Expansion Item PS-5 Liberty-Graceville 115kV TL Build new 27 mile 115kV 795 ACSR transmission line. Provide an additional source line to the area to help support voltage for certain N-2 contingencies. 2016

Liberty-Graceville Build 27 miles of 115kV, 795 ACSR transmission line

Questions?