Maharashtra State Load Despatch Centre. Partial Grid Disturbance in Mumbai system on 18 th Nov-2010 at 17:45 hrs and 21 st Nov-2010 at 17:10 hrs

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Maharashtra State Load Despatch Centre Partial Grid Disturbance in Mumbai system on 18 th Nov-2010 at 17:45 hrs and 21 st Nov-2010 at 17:10 hrs

Maharashtra State Load Despatch Centre Partial Grid Disturbance in Mumbai sub-urban system on 18 th Nov-2010 at 17:45 hrs

Maharashtra System Conditions (Prior to Disturbance) State Catered Demand : 13007 MW State Generation : 9583 MW Central Sector (Receipt) : 3424 MW System Frequency : 49.76 Hz Mumbai System Mumbai Catered Demand : 2592 MW TPC Hydro : 186 MW TPC Thermal : 1257 MW R-Infra Thermal : 498 MW Exchange with MSETCL : 658 MW

System Conditions (Prior to Disturbance) [Contd Transmission Equipments Out: 220 kv Salsette {TPC-T} Bus- Coupler : status OPEN Bus-Coupler is normally kept open in order to control loading on 220 KV Kalwa-Salsett D/C 220 kv Borivali {MSETCL}- Borivali {TPC} : status OPEN Flow on this line normally remains above 300 MW and during Mumbai peak 380 MW. Major source to Borivali is from Kalwa S/s During forced outage of ICT-1 at Kalwa line kept off from 19 th Oct. 220 kv Kalwa - Borivali {MSETCL}: status OPEN - planned outage for numerical relay commissioning

System Disturbance Following lines and units tripped, 1] 220 KV Trombay-Salset-I at 17:39 followed by tripping of following lines at 17:45 hrs 2] 220 KV Trombay-Salset-II 3] 220 KV Boisar(MSETCL)- Dahanu(R) 4] 220 KV Boisar(MSETCL)-Versova(R) 5] 220 KV Borivali(T)-Aarey(R)-I 6] 220 KV Borivali(T)-Aarey(R)-II 7] 220/100 KV Borivali(M) 125 MVA ICT-I 8] 220/100 KV Borivali(M) 125 MVA ICT-II 9] 250 MW Dahanu TPS U-I (Generator) 10] 250 MW Dahanu TPS U-II (Generator)

System Disturbance Sequence of Events of disturbance in Mumbai suburban system on 18.11.2010 Sr No Time Sequence Events 1 17:39:17 At 17:39:17:852 Hrs 220 kv Trombay-Salsette ckt-1 carrying 170 MW, tripped on phase to phase fault caused due to kite string in span 70-71 at Tagorenagar, Vikroli. 2 17:44:43 At 17:44:43:868 Hrs 220 kv Trombay-Salsette ckt-2 carrying 290 MW, tripped at 220 kv Salsette end. Earlier both the lines where carrying 170 MW each. 3 Prior to tripping, at 220 kv Salsette, Bus coupler was off.

System Disturbance (contd.. Sequence of Events of disturbance - (Contd.) Sr No Time Sequence Events 4 5 17:44:44 R-Infra system remain connected to Borivali(Tata) and further to Borivali(MSETCL) on 100 kv BO-BO Lines. Borivali(T) started drawing from Borivali(M) on 100 kv Borivali, due to network configuration. 220/100kV, 2X125 MVA ICT s at MSETCL Borivali, which were carrying 180 MW (Pre fault loading) tripped on over load. 6 Due to tripping of Borivali ICT, Borivali(T) load shifted on Reliance network. 7 This has resulted in reversal of power flow from 190 MW, from Borivali(T) to RInfra Aarey to 274 MW export from RInfra Aarey to Borivali(T).

System Disturbance (contd.. Sequence of Events of disturbance - (Contd.) Sr No Time Sequence Events 8 9 17:45:19 10 17:45:19 11 17:45:20 Reliance network was carrying about 950 MW with a Dahanu generation of 498 MW. Reliance system remained connected to Boiser(M) system. Drawal from Boisar(M) increased and 220 kv Boisar-Versova carrying 319 MW and 220 kv Boisar-Dahanu carrying 229 MW consequently tripped on Load of @ 950 MW remained connected to Reliance network having source of 498 MW, which resulted in dipping of frequency at 17:45:19:563Hrs, Automatic load shedding of @ 400 MW was initiated at 48.00 Hz. Due to further frequency dipping to 47.6 Hz, islanding scheme at Aarey operated resulting in tripping of both TPC lines at Aarey at 17:45:20:252 Hrs

System Disturbance (contd.. Sequence of Events of disturbance - (Contd.) Sr No Time Sequence Events 12 13 17:45:37 14 17:45:39 Due to load throw off on account of loadshedding on U/f and disconnection of TPCL lines at Aarey, frequency shotup to 51.75 Hz of islanded system. During these frequency oscillations, the GT-1 at Dahanu TPS tripped on overspeed at 17:45:37 Hrs. Dahanu unit 2 remained in service with the island load of @ 370 MW. Thereby tripping on under frequency at 17:45:39 Hrs. 15 Thus Total AC failure in R Infra network was of 770 MW.

System Disturbance (contd.. Sequence of Events of disturbance - (Contd.) Sr No Time Sequence Events 16 17:46:21 220 kv Bus coupler at 220 kv Salsette was closed at 17:46:21:564 Hrs and supply to Borivali(T) restored. 17 Total restoration at 19:04 hrs 664MW load was restored in Rel Infra system (400 MW from TPCL and 264 MW from Boisar) 18 Unit-2 synchronized at 2014 hrs and Unit-1 synchronized at 21:18 hrs.

(Scenario-1) : 1730 Hrs

(Scenario-2) 17:39:17 Hrs

(Scenario-3) 17:44:43 Hrs

(Scenario-4) : 17:44:44 Hrs

(Scenario-5) 17:45:19

(Scenario-6) 17:45:20

(Scenario-7) 17:45:39

(Scenario-8) 17:46:19

System Restoration 1] 220 KV Trombay-Salsette-II taken in service at 17:48 hrs 2] 220 KV Borivali (T)-Aarey (R)-I at 17:55 hrs (Aarey sub-station restored) 3] 220 KV Boisar (MSETCL)- Dahanu(R) at 18:03 hrs (aux supply todtps) 4] 220 KV Trombay-Salsette-I at 18:12 hrs 5] 220 KV Boisar (MSETCL)-Versova (R) at 18:15 hrs 6] 220/100 KV Borivali(M) 125 MVA ICT-I at 18:06 hrs 7]220/100 KV Borivali(M) 125 MVA ICT-II at 18:10 hrs At 19:04 hrs 664 MW load was restored in R-infra system. (400 MW from TPCL and 264 MW from Boiser). DTPS U-2 syn.at 20:14 hrs. DTPS U-1 syn.at 21:18 hrs.

Maharashtra State Load Despatch Centre Partial Grid Disturbance in Mumbai system on 21 st Nov. 2010 at 17:10 hrs

Maharashtra System Conditions (Prior to Disturbance) State Generation : 9093 MW State Catered Demand : 10675 MW System Frequency : 50.08 Hz Mumbai System TPC Hydro : 0 MW TPC Thermal : 936 MW R-Infra Thermal : 496 MW Exchange with MSETCL : 360 MW Mumbai Demand : 1792 MW

Disturbance on 21 st Nov. 2010 Following lines tripped 220 KV Trombay-Dharavi-V & 220 KV Trombay-Salsett-II tripped on fault at 1705 Hrs. 220 KV Trombay-Dharavi VI tripped at 1710 Hrs. This has resulted in failure of 220 KV supply to Dharavi S/s and tripping of other 110 KV lines on over load causing shut down to Dharavi S/s Bhira plant not working due to work in tailrace by irrigation department. No source to Dharavi on 220 KV Bhira-Dharavi D/C 220 KV Dharavi Backbay supply failed at Backbay.

Disturbance on 21 st Nov. 2010 Conti Area affected Load at Dharavi Load fed from Dharavi at Vikhroli Load fed from Dharavi at Mahalaxmi Load fed from Dharavi at Backbay Total Load affected Supply affected in full or partial in the part of 299 MW -- 67 MW -- 30 MW -- 29 MW -- 425 MW Marin Drive, Mantralaya, Backbay, Nariman point, Cuff parade, Colaba, lower Parel Mahalaxmi, Chinchpokali,Bomaby central Lalabag, Dadar, Mahim, Matunga, Sion, Dharavi, Bandra, Kurla, Ghatkopar, Vikroli, Chunabhatti, Mankhurd, Chembur

Disturbance on 21 st Nov. 2010 Conti 17:14 Hrs supply extended to Mahalaxmi from 110 KV Parel and about 30-35 MW load restored 17:23 110 KV Trombay-Dharavi II taken in service 17:27 220 KV Trombay-Dharavi VI taken in service 17:28 110 KV Dharavi-Vikroli taken in service 17:30 Hrs supply extended to Backbay from 220/110 KV Crnac S/s about 35 MW load restored including Mantralaya

Disturbance on 21 st Nov. 2010 Conti 17:32 Railway feeders at Dharavi & Vikroli charged Central Railway section from Chinchpokali to Mulund & Western Railway section from Dadar to Vileparle affected during 17:10 to 17:32 Hrs for about 22 min. 17:52 Hrs 220 KV Trombay-Dharavi V taken in service 18:01 Entire load at Dharavi & Vikhroli restored 18:02 220 KV Trombay-Salsett taken in service 19:49 110 KV Dharavi Mahalaxmi taken in service

Thank You