Case Study #8. 26 th Texas A&M International Pump Users Symposium March, Malcolm E. Leader Kelly J Conner Jamie D. Lucas

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Evaluating and Correcting Subsynchronous Vibration In Vertical Pumps Case Study #8 26 th Texas A&M International Pump Users Symposium March, 2010 Malcolm E. Leader Kelly J Conner Jamie D. Lucas

Case Study Overview New Vertical Pumps Liquid Sulfur Service Operating Speed 3,575 RPM Primary Vibration Component at 1,750 CPM Shaft Whirling or Whipping Suspected Structural Resonance near ½ X Solution

Pump Layout 164 Inches

Pump System 6 Vertical Pumps in 3 Separate Sumps Single Stage 81 GPM 219 Ft Head 40 HP Molten Sulfur at 300 F Pump and Shaft are Steam Jacketed 4 Radial Bearings/Bushings Top Bearing is also Thrust Bearing Line Shaft Bushings are Carbon Graphite

History Hard Sulcrete Buildup in Sumps New Pump Mounting System Devised Initial Base Impact Test Showed Structural Natural Frequency in Excess of 5,000 CPM Initial Vibration Readings: First Installation had 0.2 IPS at 1,710 CPM Second Installation had 0.65 IPS at 1,750 CPM

Vibration Measurements High Vibration on All Units Virtually no 1X (Running Speed) Vibration Most Vibration near ½X Running Speed Measured Spectrum on Motor

History Installed Impact Test Results on Motor Bump Test Location East - West Direction North - South Direction East Pump 1,734 CPM 1,887 CPM West Pump 1,657 CPM 1,887 CPM

History Clearly There was a System Natural Frequency near Half of Operating Speed What was the Forcing Function? Sulfur whirl Considered

Initial Attempts Reduced Weight of Coupling No Significant Effect Possibly Stiffen Structure? Probably would be Ineffective Not Done Rotordynamics Analysis Selected Approach

Rotordynamics Analysis Gather Data from Disassembled Unit Dimensions and Weights of all Rotating Parts Evaluate Bushing Dimensions Determine Properties of Liquid Sulfur Translate into Finite Element Model Match Model to Observed Vibrations Design New Components to Fix Problem

Actual System Compared to Model FEA Model Thrust Bearing Imbalance Top Bushing Lower Bushing 2.5 Inch Diameter Shaft 164 Inches Pump Bearing Imbalance

Center Two Rotating Sleeves Original Design Modified Design

Properties of Molten Sulfur Unusual Material Room Temperature Sulfur is a Crystalline Solid Fully Liquid at 235 F Forms Long-Chain Molecules Gamma Sulfur Highly Non-Linear Viscosity 7.8 cp at 300 F 93,000 cp at 350 F Sump Temperature Control Very Important

Crystalline Solid Sulfur

Sulfur Viscosity v. Temperature

Original Bushing Design Diametral Clearance 16 Mils = 0

First Critical Speed Mode Shape Calculated Frequency = 1,770 CPM With Original Upper and Lower Bushings

Original Unbalance Response Calculated Response At Lower Bushing 1,785 CPM

Stability with Original Bushings

Stability with Original Bushings Non-Linear Time Transient Analysis Calculated Spectrum At Lower Bushing

Evaluation Shaft Critical Speed at ½ Operating Speed Structural Resonance at ½ Operating Speed Inherently Unstable Plain Circular Bushings Need To Control The Rotor Vibration Center Two Bushings Logical Items to Revise

Solution Goals Design New Upper and Lower Bushings Increase Direct Stiffness Raise Critical Speed above Operating Speed Eliminate Instability Assure Low Operating Speed Vibration Increase Reliability and Reduce Costs

Optimized Bushing Design Diametral Clearance 9 Mils

Optimized Bushing Pressure Profile Peak Pressure 27 PSI

Bushing Stiffness and Damping Coefficient Comparison at 3,575 RPM Bushing Type Principal Stiffness, LB/IN Principal Damping, LB-SEC/IN Cross-Coupled Stiffness, LB/IN Horsepower Loss Plain Bushing 3-Lobe Bushing 1,830 407-69,400 0.65 49,100 323-20,700 0.38 (26.8 Times Stiffer)

New Design Unbalance Response Calculated Response At Lower Bushing

Stability with New Design Bushings Time Transient Analysis Time Transient Calculated Spectrum At Lower Analysis Bushing

Final Result Measured Spectrum on Motor

Conclusion Vibration Problem Eliminated Replaced 2 Plain Bushings with Profile Design Inexpensive Available Locally Eliminated Critical Speed No Structural Modifications Necessary Reliability Increased and Costs Reduced