A Prototype Oil-Less Compressor for the International Space Station Refrigerated Centrifuge

Similar documents
The Design Aspects of Metal- Polymer Bushings in Compressor Applications

A Two Stage-Double Acting Scroll Air Compressor

Transient Thermal Analysis of Screw Compressors, Part III: Transient Thermal Analysis of a Screw Compressor to Determine Rotor-to-Rotor Clearances

An Experimental Analysis on the Flow Rate in Scroll Compressors

Scroll Expander for Carbon Dioxide Cycle

Elimination of Instability in Modulating Capacity Reciprocating Compressor

Availability Analysis For Optimizing A Vehicle A/C System

Structural Analysis Of Reciprocating Compressor Manifold

CFD Analysis of Oil Discharge Rate in Rotary Compressor

Research And Development Of Variable-Speed Scroll Compressor

Numerical Simulation and Performance Analysis of Rotary Vane Compressors for Automobile Air Conditioner

Twin Screw Compressor Performance and Its Relationship with Rotor Cutter Blade Shape and Manufacturing Cost

Development of Scroll Compressor for 16HP VRF System

Infinitely Variable Capacity Control

Development of a Low Noise Rotary Compressor

Theoretical and Experimental Investigation of Compression Loads in Twin Screw Compressor

A Large Modern High Speed Reciprocating Compressor

Research of the Effectiveness of Use of New Mechanism in Reciprocating Compressors

A Novel Automotive Two-Stage A/C Compressor

Performance Improvement of a Reciprocating Air Microcompressor

The Performance Optimization of Rolling Piston Compressors Based on CFD Simulation

Comparing FEM Transfer Matrix Simulated Compressor Plenum Pressure Pulsations to Measured Pressure Pulsations and to CFD Results

Small Oil Free Piston Type Compressor For CO2

Transmission Error in Screw Compressor Rotors

Influence of Cylinder Bore Volume on Pressure Pulsations in a Hermetic Reciprocating Compressor

Development of DC Inverter Scroll Compressor used for Marine Container Refrigeration Unit

Optimum Rotor Geometrical Parameters in Refrigeration Helical Twin Screw Compressors

Developing a Compact Automotive Scroll Compressor

Diesel-Driven Compressor Torque Pulse Measurement in a Transport Refrigeration Unit

Development of a New Type Cylinder Head for Piston Compressors

Reduction of Oil Discharge for Rolling Piston Compressor Using CO2 Refrigerant

Experimental Study Of The Oil Injection Screw Air Compressor

Investigation of Torque-Fluctuation Reducer Made of Permanent-Magnets for Screw Compressors

Development of Highly Efficient Compressor Series Driven by IPM Motors

The Digital Simulation Of The Vibration Of Compressor And Pipe System

Study of a Novel Compliant Suspension Mechanism in Low Side Type Scroll Compressor

A Low Friction Thrust Bearing for Reciprocating Compressors

Transient Modeling of Vapor Compression Refrigeration Systems Using Measured Compressor COP

Spool Seal Design and Testing for the Spool Compressor

Development of High Performance 3D Scroll Compressor

Critical Solution Temperatures for Ten Different Non-CFC Refrigerants with Fourteen Different Lubricants

The Characteristics of LGE Linear Oscillating Motor

Effects of Refrigerant Injection on the Scroll Compressor

Twin-Screw Compressor Performance and Suitable Lubricants with HFC-134a

A New Device to Measure Instantaneous Swept Volume of Reciprocating Machines/Compressors

The Reduction of the Noise/Vibration Generated by the Discharge Valve System in Hermetic Compressor for Refrigerator

Important Parameters for Small, Twin-Screw Refrigeration Compressors

Oil Circulation Rate in Rotary Compressor: Its Measurement and Factors Affecting the Rate

Comparison Between Different Arrangements of Bypass Valves in Scroll Compressors

Developments in Dry Running Seals for Reciprocating Compressors

Development and Application of a Software Package for the Design of Twin Screw Compressors

Theoretical and Experimental Evaluation of the Friction Torque in Compressors with Straddle Bearings

Noise Reduction of Accumulators for R410A Rotary Compressors

The Influence of Discharge Ports on Rotor Contact in Screw Compressors

High Efficiency Reciprocating Compressors

Reciprocating Air Microcompressor

Three Phase Hermetic Protector Application Process

Storage, Bulk Transfer, and In-Plant Handling of Zeotropic Refrigerant Blends

Reducing the Fuel Consumption by Speed Control of the Air Conditioning Compressor

New Capacity Modulation Algorithm for Linear Compressor

Lubrication Analysis of Journal Bearings in R410A Rotary Compressor

Experimental Investigation of Sound Pressure Levels Variation During Modulation of a Compressor in a Unit Case Study

A Study On The Oil Supply System Of A Horizontal Rotary Compressor With Vane Utilized For Oil Feeding

Analysis and Development of a Turbivo Compressor for MVR Applications

Development of High Efficiency Swing Compressor for R32 Refrigerant

Extending the Operation Range of Dry Screw Compressors by Cooling Their Rotors

Development of Rotary Compressor for Highefficiency CO2 Heat-pump Hot-Water Supply System

Numerical Investigation of the Gas Leakage through the Piston-Cylinder Clearance of Reciprocating Compressors

Numerical and Experimental Research on Vibration Mechanism of Rotary Compressor

Verification of Flapper Suction-Va1ve Simulation Program

Noise Reduction in Bus A/C Systems with Screw Compressors Part II

Design and Development of a High Reliability, Oil Lubricated Compressor for a Space Borne Joule- Thomson Cryocooler

A Study on the Starting Characteristics of a Reciprocating Compressor for a Household Refrigerator

Discharge Characteristics of an Oil Feeder Pump Using Nozzle Type Fluidic Diodes for a Horizontal Compressor Depending onthe Driving Speed

Dynamic Modeling of a Poppet Valve for use in a Rotating Spool Compressor

CFD Analysis of Discharge Gas flow in Rotary Compressor for OCR reduction

Linear Compressors for Clean and Specialty Gases

Two-Stage Rolling Piston Carbon Dioxide Compressor

Application of Manufacturing Simulation for Screw Compressor Rotors

Design Parameters to Determine Tangential Vibration of Rotary Compressor

RECOMMENDATIONS FOR USING FREQUENCY INVERTERS WITH POSITIVE DISPLACEMENT REFRIGERANT COMPRESSORS

1. (a) If a large power generating station is operating with steam at 16,000 kpa and 500 and exhausting to a condenser at, 37.6 mm mercury absolute;

Forces Analysis of Rotary Vane Compressor for Automobile Air Conditioning System

Effect of Lubricant-Refrigerant Mixture Properties on Compressor Efficiencies

Design and Development of an Old Concept Using New Material to Produce an Air Compressor

Compressor Noise Control

Theoretical and Experimental Study of an Oil-Free Scroll Vapor Expander

A Motor Designer Looks at Positive Temperature Coefficient Resistors

Background. The function of wear rings. Wear Rings. Throat Bushing

Properties of Polyvinylether (PVE) as a Lubricant for Air Conditioning systems with HFC Refrigerants?Data Update?

Low Capacity Hermetic Type Compressor For Transcritical CO2 Applications

Application of ABAQUS to Analyzing Shrink Fitting Process of Semi Built-up Type Marine Engine Crankshaft

Noise Reduction of Fractional Horse Power Hermetic Reciprocating Compressor

Stepless Variable Capacity Control

Direct Torque Measurement of Hermetic Rotary Compressors Using Strain Gauge

Characteristic of a Miniature Linear Compressor

On the Classification of Compressor,Pump or Engine Designs Using Generalized Linkages

Research on the Structure of Linear Oscillation Motor and the Corresponding Applications on Piston Type Refrigeration Compressor

Evaluation of methods to decrease the discharge temperature of R32 scroll compressor

Influence of Volumetric Displacement and Aspect Ratio on the Performance Metrics of the Rotating Spool Compressor

Transcription:

Purdue University Purdue e-pubs International Compressor Engineering Conference School of Mechanical Engineering 2000 A Prototype Oil-Less Compressor for the International Space Station Refrigerated Centrifuge L. R. Grzyll Mainstream Engineering Corporation G. S. Cole Mainstream Engineering Corporation Follow this and additional works at: http://docs.lib.purdue.edu/icec Grzyll, L. R. and Cole, G. S., "A Prototype Oil-Less Compressor for the International Space Station Refrigerated Centrifuge" (2000). International Compressor Engineering Conference. Paper 1375. http://docs.lib.purdue.edu/icec/1375 This document has been made available through Purdue e-pubs, a service of the Purdue University Libraries. Please contact epubs@purdue.edu for additional information. Complete proceedings may be acquired in print and on CD-ROM directly from the Ray W. Herrick Laboratories at https://engineering.purdue.edu/ Herrick/Events/orderlit.html

A PROTOTYPE OIL-LESS COMPRESSOR FOR THE INTERNATIONAL SPACE STATION REFRIGERATED CENTRIFUGE Lawrence R. Grzyll and Gregory S. Cole Mainstream Engineering Corporation 200 Yell ow Place Rockledge, Florida 32955 ABSTRACT Under a subcontract from Lockheed-Martin Space Operations, Mainstream Engineering Corporation has successfully designed, fabricated, and tested a new oil-less hermetic reciprocating compressor that will operate in a zero-gravity environment. This compressor is used in a refrigerated centrifuge, which will be placed on the International Space Station. The original centrifuge used an oil-lubricated hermetic reciprocating compressor that was unsuitable for use in the zero-gravity space environment. The prototype oil-less compressor was a modified version of the hermetic reciprocating compressor used in the refrigerated centrifuge. Exhaustive orientation and performance testing of the modified compressor was performed. Life testing of the prototype compressors is underway. INTRODUCTION Lockheed-Martin Space Operations (LMSO) is in the process of developing a refrigerated centrifuge for use on the International Space Station (ISS). A commercial off-theshelf (COTS) refrigerated centrifuge has been selected for use. The COTS refrigerated centrifuge uses a R-404A vapor compression refrigeration system with a hermetic reciprocating compressor that has gravity-dependent lubrication unsuitable for use in space. Lockheed-Martin Space Operations commissioned a subcontract to Mainstream Engineering Corporation to design, fabricate, and test a prototype retrofitted compressor that will operate in a micro-gravity environment. Mainstream modified the existing compressor, performed orientation testing of the modified compressor, performed performance testing of the modified compressor, compared the performance of the modified compressor to the unmodified compressor, and initiated life testing of modified compressors to demonstrate 4000 hours of successful operation. The prototype compressor had to meet several requirements related to performance, life, and reliability. First, the prototype compressor should have similar performance characteristics to the unmodified compressor, as measured by system capacity and power consumption. Second, the prototype compressor should be mounted in the centrifuge and operate satisfactorily for one hour on each of the six sides of the centrifuge. Third, the prototype compressor should demonstrate an operational life of 4000 hours with a 90% duty cycle. 121

DESCRIPTION OF COMPRESSOR MODIFICATIONS Many design modifications were incorporated into the prototype compressor to ensure suitable operation and performance in a micro-gravity, oil-less environment. A summary of the modifications is provided below, followed by a detailed discussion of the modifications. A self-lubricating polyimide sleeve was inserted into the cylinder bore (after opening the diameter of the bore to accommodate the sleeve). Polyimide thrust washers were used to replace the oil-lubricated thrust washers. Sealed roller bearings were installed on the crankshaft and connecting rod. These sealed, permanently lubricated bearings replaced the existing oil-lubricated bearings. An oil-impregnated bronze sleeve bearing was used on the wrist pin. The connecting rod and bearing plate were redesigned and fabricated to accommodate the sealed roller bearings. A modified two-piece crankshaft was fabricated to accommodate the connecting rod and bearings. The two-piece crankshaft was hardened, press fit together, and ground to final dimensions. Modifications to the compressor/enclosure mounts were made for suitability in various gravity orientations. The existing springs were replaced with hard mounts, which were welded into place. Modification of the discharge line was made to eliminate potential failure in a discharge line muffler joint. The discharge line muffler was eliminated. Polyimide Sleeve The polyimide resin used for the sleeve and thrust washers contained 15% by weight graphite filler, which is added to reduce wear and friction. An analysis of the polyimide sleeve, which is press-fit inside the cylinder bore, was performed to confirm proper fit and dimensions in both high and low-temperature conditions. High temperature conditions will result in swelling of the sleeve, cylinder, and piston, and could cause interference at the sleeve/piston clearance. Low temperature conditions could cause the sleeve to shrink more than the cylinder bore, resulting in a sloppy fit of the sleeve in the bore. This analysis resulted in a range of allowable sleeve dimensions that would be suitable for both high and low temperatures. Crankshaft and Connecting Rod Modifications The existing crankshaft and connecting rod of the compressor were sent to an outside lab for material identification. The crankshaft was fabricated from cast iron and the connecting rod was fabricated from 3 80 aluminum casting. Also the hardness of the crankshaft, piston, arid wrist pin were measured and determined to be 88 HRB, 65 HRB, and 59 HRC, respectively. Mainstream selected a modified, vacuum-hardened, 4340 steel to fabricate the crankshaft and 6160-T6 aluminum to fabricate the connecting rod. No modifications to the piston were made. In order to accommodate the modified connecting rod and sealed bearings, redesign of the crankshaft was required. A two-piece split crankshaft was necessary in order to adequately install the bearings and connecting rod on the shaft. The two-piece crankshaft was designed to have a profile that matched the existing crankshaft. The two shaft pieces are press fit with a class FN2, "medium-drive" interference fit. An alignment hole, pin, and connecting bolt were 122

also installed to aid in proper alignment and fit. The crankshaft was machined to preliminary dimensions, hardened, and ground to final dimensions prior to final assembly. Finite element analysis of the crankshaft was performed to analyze the bending of the shaft at full load to confirm that it was in tolerable limits. COMPRESSOR PERFORMANCE TESTING The performance of the unmodified and prototype compressors was measured on Mainstream's heat pump test stand, details of which have been described elsewhere (Ref. 1). Mainstream's test stand incorporates two independent temperature controlled water loops, one to supply the heat load to the evaporator and one to remove heat from the condenser. The heat load supplied to the evaporator is determined from the measured flow rate and temperature difference of the water loop. Compressor power is measured directly. In order to simulate the operating conditions of the refrigerated centrifuge, the water temperature supplied to the evaporator was controlled to sac and the water temperature supplied to the condenser was controlled to 32 C. Unmodified Compressor Performance Eight unmodified compressors, identical to those in the COTS refrigerated centrifuge, were performance tested. Table 1 provides the average performance results for the compressors. Table 1 -Performance Results for Unmo<lified Compressors Performance Parameter Average Value Suction Pressure 478 kpa Discharge Pressure 1.65 MPa Evaporator Exit Superheat 6.2 oc Condenser Exit Subcooling 3.8 oc Compressor Power 553 w Cooling Capacity 879W COPe 1.59 Initial Verification Testing of Prototype Compressor Initial verification testing of prototype compressor # 1 was performed using an unhardened crankshaft that was machined to final dimensions (this decision was made to save time, since the hardening and grinding process required considerable time). During the initial verification testing, the compressor ran nominally for approximately 20-25 minutes. At that time, the compressor power rose significantly, resulting in the compressor overload protection engaging, stopping the compressor. An audible slowing of the compressor speed was observed during this event. It appeared that a significant amount of friction resulted in excessive heat generation and torque requirements. 123

Initial attempts to correct the problem focused on the piston/bore clearance. This clearance was gradually increased from an initial value of 0.0007 inches to 0.0017 inches. Increasing the piston/bore clearance, however, did not correct the problem. The compressor was then disassembled. Inspection showed that the motor rotor and stator were rubbing. The friction and heat from this rubbing caused the compressor overload protection to shut the motor off. The potential causes of this were bearing misalignment, crankshaft deflection, and/or thermal expansion ofthe rotor/stator. Further inspection of the compressor revealed some displacement of the crankshaft due to bearing play and misalignment. Misalignment of the bearings was corrected using precision shoulder screws to align the bearing plate. The bearing clearance is 0.0008-0.0016 inches, which contributes to the rotor touching the stator. Some deflection of the crankshaft at full load conditions also contributed to the problem. The rubbing of the rotor and stator was confirmed using temperature indicators on the compressor components. Temperature indicators on the stator showed temperatures in excess of 215 C. Temperature sensors on the cylinder head and housing indicated temperatures of approximately l20 C. Methods to minimize the bearing clearance were investigated. This could be accomplished by grinding the OD of the crankshaft to match the bearing ID. However, this method would require an exact measurement of the bearing ID using a plug gauge, which would require selection of the appropriate plug gauge with the correct diameter. This is not practical due to the variation in bearing tolerance. It was also believed that this would not likely diminish the shaft displacement. We next investigated modifications to the stator. We added alignment pins where the stator fastened to the compressor housing to minimize the play between the stator and housing. We investigated opening the ID of the stator magnets using a honing stone. Our approach was to open the stator ID in 0.002 inch increments radially. Significant improvement was seen in the first 0.002 inch increment. The second 0.002 inch increment appeared to eliminate the problem, resulting in several experiments of duration of2-3 hours each, without motor shut-down. Upon further verification testing and inspection, we noticed that the connecting rod had cracked due to the piston hitting the head. Inspection of the machined crankshaft showed significant deflection, contributing to the piston hitting the head. Replacement of the machined crankshaft with the hardened, ground crankshaft eliminated this problem. Performance Testing of Prototype Compressors A second prototype compressor was fabricated using the same modification as the first prototype compressor. Prototype compressors # 1 and #2 were then tested on the heat pump test stand using the same water supply temperatures as the unmodified compressors. Table 2 summarizes the performance of the prototype compressors along with the average performance of the unmodified compressors. 124

Table 2 - Compressor Performance Comparison Unmodified (Avg. of8) Prototype #1 Prototype #2 Power Consumption 533 w 551 w 575W Cooling Capacity 879W 705W 832W COPe 1.59 1.28 1.45 Suction Pressure 478 kpa 503 kpa 502 kpa Discharge Pressure 1.65 MPa 1.52 MPa 1.63 MPa Evap. Superheat 6.2 oc 4.8 oc 5.1 oc Cond. Subcooling 3.8 oc 0.4 oc 3.2 oc Table 2 shows that the performance of the modified compressor is only slightly lower than the unmodified compressor. Power consumption rose 3.4%, which is considered negligible since it is within 2 standard deviations of the average power consumption of the unmodified compressors (see Table 1). Cooling capacity dropped 19.5%. The drop is cooling capacity is likely the result of a reduction in compression efficiency, caused by two phenomena: 1. The piston/bore clearance in the modified compressor, which was increased from 0.0007 inches to 0.0017 inches during verification testing. The piston/bore clearance in the unmodified compressors is 0.0007 inches. This increased clearance results in leakage around the piston during the compression process, resulting in less gas getting compressed with each stroke, lowering cooling capacity. 2. The discharge temperature of the modified compressor was higher than the unmodified compressor (approximately 190 F versus 132 F). This is an indication of increased friction in the modified compressor, converting some of the power supplied to the compressor to heat, thus lowering the compression efficiency. This is not a surprising result, since oil lubrication is preferred over the sealed bearings, a polyimide lubricated piston, and a polyimide thrust washer used in the modified compressor. 3. The clearance volume when the piston is at top-dead-center may be greater in the modified compressor. During verification testing, some material was taken off the piston, which would increase this clearance volume. This would decrease the volumetric efficiency of the compressor. COMPRESSOR ORIENTATION TESTING The modified compressor was installed in the COTS centrifuge for orientation testing. The refrigeration system was charged with 170 grams ofr-404a refrigerant (the factory charge). For orientation testing, the set point of the centrifuge was set at 6 C. The centrifuge was operated for one hour on each of the six sides of the centrifuge. The test objective was to confirm proper operation at all orientations and to monitor the total compressor run time and duty cycle (the compressor cycled on and off during the test). After each test, the centrifuge was allowed to warm up to room temperature prior to initiation of the following test. 125

Table 3 shows the results of the orientation tests, showing the total compressor run times and duty cycle for each orientation. The variation in the total run time and duty cycle seen in Table 3 for the various orientations is the result of the effect of gravity orientation on the performance of the condenser and capillary tube expansion device. The condenser is designed to operate in an orientation with gravity where the vapor enters at the highest location and the liquid leaves at the lowest location. Thus, liquid flows in a direction where it is assisted by gravity, supplying subcooled liquid to the capillary tube. As the centrifuge was place in other gravity orientations, liquid was forced to flow against gravity. This could result in hold-up of the liquid at a low spot in the condenser, resulting in a two-phase liquid-vapor mixture entering the capillary tube (since vapor flows against gravity much easier than liquid). This would decrease the cooling capacity of the refrigeration system, since the refrigerant entering the evaporator would have a higher vapor quality than intended. This explains difference in compressor run times and duty cycles for the various orientations with gravity. Table 3-Orientation Testing Results Orientation Total Run Time Duty Cycle Upright 22 min. 36.7% Left Side 45 min. 75.0% Right Side 46 min. 76.7% Top Down 34 min. 56.7% Back Down 60 min. 100% Front Down 22 min. 36.7% COMPRESSOR LIFE TESTING The purpose of compressor life testing was to demonstrate that the modified compressors could operate for 4000 hours at a 90% duty cycle. The life test stands consist of a modified compressor, an air-cooled heat exchanger, a commercial filter-drier, and a hand expansion valve. Thus, the life test cycle is a vapor cycle. The test stand is instrumented with thermocouples on the compressor suction line, discharge line, and compressor body. Pressure gauges are installed on the compressor suction and discharge lines. The refrigerant charge and hand expansion valve are adjusted to provide a suction pressure of approximately 480 kpa and a discharge pressure of approximately 1.55 MPa. An hour meter and timer are installed on the compressor's electrical supply to monitor and control the compressor run time. The timer is set so that the compressor is on for 15 minutes, 40 seconds and off for 1 minute, 43 seconds. This is a 90.12% duty cycle, and will provide 15,318 cycles over the 44 3 8 hours of testing. Life testing of the compressors is currently underway. 126

CONCLUSION Mainstream successfully modified and tested an oil-less compressor for operation in a zero-gravity environment. Performance testing of the modified compressors showed negligible difference in power consumption compared to the unmodified compressors and only a 19-20% decrease in cooling capacity and COPe. Orientation testing was successful in demonstrating operation of the compressor in all six gravity orientations. Life testing, to demonstrate 4000 hours of operation at a 90% duty cycle, is underway. REFERENCES 1. Grzyll, L. R., Scaringe, R. P., and Gottschlich, J. M., "The Development of a Performance Enhancing Additive for Vapor-Compression Heat Pumps," Proceedings of the 32nd Jntersociety Energy Conversion Engineering Conference, 1252-7, 1997. 127

128