Clay McClinton Rotating Equipment Reliability Analyst, Chevron. Dan Phillips Manager Global Field Services, Kop-Flex

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COUPLING FAILURE DUE TO A MOTOR FAULT

COUPLING FAILURE DUE TO A MOTOR FAULT Clay McClinton Rotating Equipment Reliability Analyst, Chevron Dan Phillips Manager Global Field Services, Kop-Flex Joe Corcoran Manager Global Services & Training, Kop-Flex

Incident Description Soft Start Synchronous Electric Motor driving a Speed Increasing Gearbox to a Centrifugal Compressor Running since 2003 with no significant issues; Last shutdown in 2008 Motor / Diaphragm Coupling /Gearbox 15,000 hp @ 1,200 rpm (682,800 lb-in) Gearbox/ Disc Coupling / Compressor 10,790 hp @ 6,662 rpm (102,100 lb-in) During start-up following 2013 turnaround, speed of motor dropped several times coming up to speed Some electrical maintenance performed on motor during turnaround Failure and ejection of high speed coupling occurred 12 seconds after start (main part went 70 yards) No injuries 3

Motor Speed Data from LS Speed Pick-up Speed Abnormality 4

Broken Guard Due to Ejected High Speed Coupling Center Section 5

Failed Components Less Rigids Comp. Side Coupling Spacer note 45 angle GB Side Disc and bolt fragments Spacer Flange, comp. side 6

Spool Piece from Gearbox Side 7

Spool Piece from Compressor Side Note: threaded portion of bolts bent in direction of rotation Note Anti-Flail Did Not Contain 8

Driving End of Spacer with Nut Broaching Nut/bolt pulled through flange 9

Waterfall Plot from Start Up Reveals 6.9 Mils @ 11.25 Hz Data from gearbox 6X radial probe, low speed side Prior to shutdown, radial vibration was <0.5mils p-p 10

RCA No conclusive evidence of liquid slug High speed coupling flange bolts intact Failure <5.8X normal torque, based on bolt strength with flange friction Shear Stress >84,000 psi on spacer tube >6X normal torque to yield Additional bending loads occurred as disc pack buckled Disc pack buckled, bolts bent Max momentary rating of HS coupling 3.3X normal torque 3.3X normal torque < Failure Torque < 5.8X normal torque 11

Evaluation Location of initial failure was on compressor end of HS coupling center section Scenario Comp. end disc pack buckles, disc pack bolts bend Comp. end flange/tube breaks due to torque + bending loads Remaining portion of center section breaks through anti-flail Unbalance forces (>30,000 lb) rip center section away from opposite end disc pack Kinetic energy of broken center section (~4300 ft-lb f ) allows ejection through coupling guard 12

Evaluation Low speed coupling looked good visually Replaced as precautionary measure. Further inspection revealed no defects. Low speed coupling had higher torque capacity ratio Max Momentary Torque was 8X vs. 3.2X Not typical Original Selection was a MAX-C Elastomeric Coupling So what caused the tremendous loads? Speed fluctuations investigated Torsional analysis reviewed 13

Motor Speed Data from Solo Run Loose wire found on motor diode wheel Uncoupled solo run of motor confirmed speed abnormality 14

Loose Wire Repaired; Motor Speed Data from Successful Start up 3/26 Motor wiring corrected Second solo run showed no speed fluctuations 15

Coupled and Solo Run Electrical Data Current Fluctuations Source of Excitation 3 2 1-2008 Start-up 2- Failure Event 3- Solo run, before repair 4- Solo run, after repair 5- Successful start up 4 5 1 16

Verification of Torsional Analysis Original torsional analysis reviewed Frequency (11.25 Hz) of high radial vibrations found during start-up prior to failure appeared to be near a system torsional natural frequency New forced response analysis conducted Wiring problem caused current fluctuations in motor, exciting torsional natural frequency Need to determine effect of short duration torsional excitation at motor, resulting from diode wheel wiring 17

Campbell Diagram 1 st Torsional Mode at 11.9 Hz (719 CPM) 18

Calculated Torque on Coupling During ~4X Rated Resultant torque coincides with predicted failure torque levels 3.3X normal torque < Failure Torque < 5.8X normal torque TAF response of high speed coupling with 0.5 sec excitation of first natural frequency applied at motor,.013% damping included. 19

Vibration Data from Successful Start- up 3/26 20

Lessons Learned and Recommendations This is a Very Rare Occurrence that Could Have Been Prevented Conduct Torsional Vibration Analysis- Forced Response Faulty motor wiring excited torsional natural frequency during start-up TVA concluded that peak torques exceed coupling rating and also TVA provides critical information on location of weak point and can be used to evaluate necessary change (mass-elastic properties, overload protection, etc.) Wiring Checks After any motor electrical maintenance, a full inspection of wiring connections is required Perform solo run on motor after major electrical maintenance completed Different couplings could have helped - Larger High Speed Coupling or Shear Section at High Speed (or Low Speed?) Unnecessary personnel should never be in close proximity to rotating equipment during start-up 21