Vibration Signature Analysis as a Diagnostic Tool for Condition Assessment of Rotating Equipments Experience at TAPS

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56 Vibration Signature Analysis as a Diagnostic Tool for Condition Assessment of Rotating Equipments Experience at TAPS S.K. Acharya a, Amalendu Das a, V.K. Gupta a, K.R. Anilkumar a, Ravindranath b and S. Bhattacharjee c a Technical Services Section, TAPS 1&2 b Chief Superintendent, TAPS 1&2 c Station Director, TAPS 1&2 Tarapur Atomic Power Station 1&2 Proceedings of the National Seminar & Exhibition on Non-Destructive Evaluation Email : skacharya@npcil.co.in, vkgupta@npcil.co.in NDE 2009, December 10-12, 2009 ` Abstracts Tarapur Atomic Power Station 1&2 (TAPS # 1&2) is a twin Boiling Water Reactor (BWR) nuclear power station, with each unit operating at 160 MWe. Both the units were commissioned in November 1969 and completed about 40 years of operation. Nuclear power plant operation requires reliable and continuous operation of equipments confirming to its design intent. These equipments include rotating equipment (such as pumps, compressor, turbine generator, fan etc) and static equipments (such as heat exchanger, reactor vessel). TAPS has adopted reliability centered maintenance (RCM) policy for rotating equipments. To execute RCM performance data such as operating parameters, vibration, bearing temperature, noise, speed and current are monitored. Based on parameters condition assessment of equipment is done. This allows us to schedule the maintenance programme or other actions to be taken before the failure occurs to avoid the consequences of failure. It is typically much more cost effective than allowing the machinery to fail. By following these tools TAPS has been able to operate in safe, efficient and economical manner. For judging rotating equipments condition, vibration monitoring and its signature analysis has significant contribution. TAPS has solve many uncommon problem of rotating equipment during last 15 years such as rectification of turbine generator thermal sensitivity, rectification of high pressure multi stage pump high noise problem, rectification of vertical turbine pump high vibration problem and many more. This paper depicts an overview of TAPS condition monitoring and performance evaluation on the basis of vibration signature analysis of rotating equipments at TAPS 1&2 with some case studies 1. Introduction Maintenance (RCM) policy for rotating equipments. To execute RCM, performance data such as operating Tarapur Atomic Power Station is a two-unit Boiling Water parameters, vibration, bearing temperature, noise, speed and Reactor (BWR). It is a dual cycle, forced circulation boiling current are monitored. Based on monitored parameters water reactor producing steam for driving steam turbine. The condition assessment of equipment is done. This allows plant schematic diagram is shown in Fig.1. TAPS is designed to produce 210 MWe but due to operational problem plant is re-rated to 160MWe since 1985 by isolating secondary cycle (Blue line in Fig. 1 showing secondary cycle). A nuclear power plant requires operation in highly safe and strict regulatory environment. Safe and reliable operation of plant equipments need continuous monitoring and regular inspection to evaluate deficiencies so that appropriate design modification or maintenance activities can be taken-up in conservative manner to improve the equipment life and system performance. In nuclear power plant operation, many important types of equipment are not accessible due to radiation hazard and operational/ technical specification requirements. There is also strict control over the outage period of the equipments which are important for the safe operation of the nuclear power plant. With all these consideration, in order to maintain safety, reliability and high plant load factor, continuous operation of equipments conforming to its design intent is required. Hence a systematic and structured maintenance program is necessary for to fulfill above requirements. TAPS has adopted Reliability Centered Fig. 1

NDE 2009, December 10-12,2009 57 scheduling the maintenance programme and to take corrective action in time to avoid the consequences of failure, before the failure occurs. It is typically much more cost effective than allowing the machinery to fail. By following these tools, TAPS has been able to operate in safe, efficient and economical manner. For evaluating rotating equipments condition, vibration monitoring and its signature analysis has given significant contribution. 2. Reliability Centered maintenance (RCM) Maintenance means correcting the deficiency of the equipment after it stops functioning so that equipments continue to do its intended function whereas reliabilitycentered maintenance is a process used to determine what must be done to ensure that any equipment continues to do what its user want it to do in its present operating condition. The RCM encompasses all types of maintenance philosophy such as break down maintenance, preventive maintenance and predictive maintenance. The RCM considers the function and performance expectation of concerned equipment and how its failure affects the plants availability and safety. It also covers what can be done to predict or prevent failure. The key issue is the reliability of the equipment and focus on Root Cause Analysis of failure. TAPS has categorized the plant equipments based on performance expectation and its reliability requirement for high plant availability without compromising on safety. Main categories are (i) Critical (required for nuclear safety) (ii) Important (will affect generation) (iii) Normal (their outage can be tolerated for a limited period). Type of monitoring and maintenance is decided based on the category of the equipment. TAPS has adopted systematic condition monitoring programme for rotating equipments such as pumps, turbine, compressor and fans. The monitoring is done either fortnightly or monthly depending on the category of the equipment. The performance parameters are trended and if any deviation in any of the parameter is noticed then detailed analysis is done to identify the probable cause. Vibration is one of the performance parameter which is monitored. The limiting value of vibration is decided based on pre-operational data of concern equipment or as per ISO-10816 or IS- 14817. If the vibration level is more than the limiting value or appreciable increase in the vibration level observed between two consecutive monitoring than vibration signature analysis is done. 3. Vibration Signature Analysis Vibration is a cyclic or pulsating motion of a machine or machine component from its point of rest. Vibration consists of amplitude (viz displacement, velocity or acceleration), frequency and phase. It represents a measurable symptom of a problem associated with rotating equipment which results in destructive mechanism such as fatigue, stress or wear of concern equipments. The nature of the developing fault has unique vibration characteristics and will be determined by comparing the vibration amplitude, phase and exciting frequencies in different radial directions of rotating equipment. Fig. 2 The worst problem usually dominates the vibration. Vibration of rotating equipments consists of different exciting frequencies. So, the time domain spectrum will be very complex to analyze. To simplify analysis, Fast Fourier Transformation is applied on the time waveform. FFT is a mathematical algorithm that synthesizes the complex time waveform into individual sinusoidal waveform contents. For each sine waveform, amplitude and period of vibration can be calculated. In turn from period of vibration, frequency of vibration can be calculated. This information is then displayed in a different format with frequency in X axis and amplitude in Y axis. This representation is known as vibration spectrum, frequency spectrum, FFT spectrum or vibration signature. A typical vibration spectrum is shown in Fig. 2. Many methods are available for vibration analysis such as Bump test, Bode Plots, Polar Plots, Cascade or water fall plots etc. These analysis tools are helpful in identifying the probable cause of high vibration and also help to decide line of action. The following paragraphs give two case studies of long pending problem of TAPS solved by systematic vibration analysis and illustrate the importance of vibration signature analysis in solving these problems. 4. CASE-1: Rectification of Unit#1 turbogenerator thermal sensitivity problem Tarapur Atomic Power Station (TAPS) # 1&2 has two turbo-generators of 210 MWe capacities each. Both the turbines are tandem-compounded, impulse type, with one High Pressure (HP) and one Low Pressure (LP) unit. HP turbine is dual admission single flow type with 18 stages and LP turbine is single admission dual flow type with 4 stages. HP and LP turbines, generator and exciter are coupled in tandem. The generator is a star connected, 3 phase, 50 cycle, 1500 RPM, four pole machine with 248 MVA rating and 12 KV voltage. Generator stator and rotor windings are cooled by hydrogen. Generator casing hydrogen pressure is maintained at 1 Kg/cm 2. Turbine-generator is supported by six hydrodynamic journal bearings. Bearings # 1&2 are for HP turbine, Bearings# 3&4 are for LP turbine and Bearings #5&6 are for generator. Vibration sensors are installed at each bearing to monitor turbine-generator shaft vibrations. As per the original design, one seismically mounted, contact

58 Acharya et al. : Proceedings of the National Seminar & Exhibition on Non-Destructive Evaluation Table 1 Year 1995 Date Generation in Mwe B#1 B#2 B#3 B#4 B#5 B#6 Remarks 20-Feb-95 160 1.5 2.5 1 0.8 2 2.5 02-Jun-95 157 1.2 1.8 1.3 0.8 2.2 2.8 1997 12-Sep-97 160 0.4 1.5 1.8 1.2 2.8 5.8 1998 31-Mar-98 160 0.5 1.8 2 0.6 2.5 6.2 2000 01-Feb-00 163 1 2.5 2 2.5 6 5 Table 2 Year Date Generation in Mwe Before swapping of unit#1 and Unit#2 generator rotors After swapping of unit#1 and Unit#2 generator rotors B#1 B#2 B#3 B#4 B#5 B#6 Remarks 2000 13-Jun-00 160 0.6 1.5 2 1.8 3.8 4.8 2001 03-Mar-01 160 6 1.8 1.8 2 4.2 5.2 2002 19-Aug-02 165 1 2 1.6 1.6 3 3.2 2003 12-May-03 160 1.5 1.5 2.5 2 4.5 5 2004 30-Dec-04 160 1.4 1 2.6 3.4 5.4 6 After dynamic (trim) balancing and putting 1.975 kg on the generator fan ring at the exciter end at 265 o location in the direction of rotation. type shaft riding velocity probe is installed on each bearing for the continuous monitoring of shaft vibrations. In addition to this, two non-contact type proximity probes of M/s Bentley-Nevada make are also installed in the X-Y direction on each bearing. Recorders are provided in control room for the continuous monitoring of turbine generator. If the vibration level exceeds the limiting value of 5 mils (127 microns), recorders will give high vibration alarm in control room to alert the operators to take appropriate corrective actions. In addition vibration monitoring is done monthly by portable vibration meter/ analyzer. In the year 1996, Unit #2 generator rotor developed ground fault. Since Unit #1 was under outage, Unit #1 generator rotor was installed in Unit #2 for early restart of Unit #2. After repair of failed generator rotor removed from the uni#2 it was installed in unit#1. After swapping the generator rotors, Unit #1 turbine generator shaft vibrations gradually increased to 5.6 mils (140 microns) at 160 MWe generation. Casing vibrations were 5 mils (127 microns) and foundation vibrations were 3.7 mils (93 microns). (Table 1) The vibration signature revealed that predominant frequency of vibration is 1 RPM and increase in the vibration of bearing #5 and bearing #6 was noticed as generator output was increases from start to full power. All these information suggest the high vibration was due to thermal sensitivity. In the mean time grouting repair of turbine generator concrete foundation and dynamic (trim) balancing of generator rotor was done to reduce the vibration level to some extent. After these works vibration level on bearing # 6 reduced to 4.8 mils at 160MWe. This had also given some times to decide when to do the generator repair work. Since generator repair work require large outage period so, it was decided to plan the generator rotor pulling for repair during up-gradation outage period Oct 2005 - Feb 2006. During this period regular monitoring of turbine generator vibration was done. However, vibration level on bearing #6 gradually increased from 4.8 mils to 6 mils. Generator rotor thermal sensitivity is a phenomenon which may occur on the generator rotor causing the rotor vibration to change as the field current is increased. The thermal sensitivity can be caused by an uneven temperature distribution circumferentially around the rotor, or by axial forces which are not distributed uniformly in the circumference. The primary driver of this second cause is the large difference in coefficient of thermal expansion between the copper coils and the steel alloy rotor forging and components. If the rotor winding is not balanced both electrically and mechanically in the circumferential direction, the generator rotor will be unevenly loaded which can cause the rotor to bow and cause the vibration to change. A thermally sensitive rotor is characterized by a once-perrevolution frequency response signature due to a change in the rotor balance arising from the rotor bow. Probable causes of thermal sensitivity in the generator are a) Blocked rotor ventilation holes or non-uniform circumferential cooling, b) variation of inter-turn insulation c) Retaining ring/centering ring assembly movement d) Heat sensitive rotor forging e) Tight slot.

NDE 2009, December 10-12, 2009 59 Fig. 4 Fig. 6 Fig. 5 In the year 2005-06, during the Unit #1 outage for plant safety upgradation, station could rectify the problem. Details of the works carried out are described in this report. Rotor was pulled out for inspection and repair. Retaining rings were removed for inspection of overhang and inter-turn insulation. Inspection and thoroughness check of Unit #1 generator rotor ventilation holes were carried out during the unit outage and generator retaining ring inspection was also done. Following were the salient observations and corrective actions taken. 1. In generator rotor winding slots # 1&40 (Coil#1) interturn insulation, which was replaced in the year 1988-89 after rotor ground fault, got displaced and hence it was blocking the ventilation holes. 2. Rotor composite insulation of slots 1&40, 29&32 and 28&33 was replaced with new insulation material of 0.3 mm ((12 mils) thickness, which is comparable with the original GE make inter-turn insulation of 0.33 mm (13 mils) thickness. Summary is given below: - Coil Slot Thickness of existing Thickness of No. No. inter-turn insulation (mm) replaced interturn insulation (mm) 1 1 & 40 0.50 0.30 (Installed in 1988-89) (Replaced in 2005-06) 2 29 & 32 0.35 0.30 (Installed in 1996-97) (Replaced in Sandwiched insulation 2005-06) of 0.15 /0.05/0.15 mm 3 28 & 33 0.35 0.30 (Installed in 1996-97) (Replaced in Sandwiched insulation 2005-06) of 0.15/0.05/0.15 mm Fig. 7 3. All the ventilation holes were checked after repair for thoroughness and found to be free from any obstruction. 4. After removal of retaining ring liquid penetrant examination and ultrasonic examination was done to check its healthiness and its condition was found to be OK in all respect. 5. High vibration of Unit #1 turbine generator was due to thermal unbalance in the rotor, caused by rotor bowing. The rotor bowing is either due to uneven cooling of rotor or inter-turn shorting due to presence of copper dust or variation of inter-turn insulation. Variation in inter-turn insulation type and thickness causes uneven friction forces between the coil and insulation.

60 Acharya et al. : Proceedings of the National Seminar & Exhibition on Non-Destructive Evaluation This result in variation of coil expansion in the axial direction due to increase in field current and causes uneven loading on the generator retaining ring subsequently rotor bow. Uneven cooling of rotor was due to blockage of ventilation holes in the rotor caused by the displacement of inter-turn insulation. In view of above taken actions, Unit #1 turbine generator vibration values are expected to be low. Therefore, on 25.01.2006 the balancing weight of 1.957 kg was removed from the generator fan ring at exciter end, at 265 o location in the direction of rotation. 4.1 Performance of turbine generator after maintenance After completion of above work, Unit #1 turbine generator was synchronized to grid on 16.02.2006. Vibration performance of the turbine generator was closely monitored during the start-up, at no load and at different loads up to 160 MWe (Refer Fig: 7A & 7B). All the vibration values were found to be within the acceptable limit. Bearing # 5 vibration was 1 mil (25 microns) and Bearing #6 vibration was 3.0 mils (76 microns) at 160 MWe. Also at Bearing #5, the maximum bearing casing vibration was 0.7 mils (17 microns) in the vertical direction. Similarly, at Bearing #6, the maximum bearing casing vibration was 2.2 mils (55 microns) in vertical direction. The generator foundation vibration has reduced from 2.9 mils (73 microns) to 1.5 mils (38 microns). All the vibrations are satisfactory and long pending high vibration problem of unit#1 turbine generator is successfully solved. This was higher than the 12 mm/sec acceptable limit for piping vibration as per ASME O & M code for nuclear piping. The vibration amplitude corresponds to pump rpm 87.5 Hz was very low. Whereas vibration peaks of high amplitude found at 365.2 Hz, 1 KHz, 1.5 KHz etc and these frequencies were not the harmonics of pump speed. These could be some of the high frequency piping mode getting excited due to turbulent flow (Refer fig:8). Vibration on and around the pump was low as compared to vibration on the suction line and bends in the piping. Discharge line vibration is lower than the suction line vibration. In the suction line near the bend prominent frequency peaks were at 325, 337, 362, 637, 700 Hz with different amplitude. The noise level around the suction line of pump 1NDO6C was in the range of 105 to 110 dba whereas noise around suction line of other unit pump (2NDO6C ) was 94 dba. Overall vibration in the suction line of 2NDO6C was low in comparison with vibration of suction line of 1NDO6C. The prominent frequency peaks in the spectrum were at 87.5, 216, 512 Hz of low amplitude. The suction and discharge nozzle of the pump is directly connected with elbows through a very small spool with length of 2.5 inches whereas same spool length in 2NDO6C 5. Case: II Rectification of High Noise Problem of High Pressure Multistage Pump Reactor water chemistry is continuously maintained by reactor clean-up system and this system consists of heat exchangers, clean-up demineralizer, filters and pumps. Reactor clean-up recirculation pump of unit#1 1NDO6C was having high noise problem since long time. The noise level near to its suction line was in the range of 105 dba. This pump is M/s KSB make Horizontal 7 stages centrifugal modular design pump, with mechanical shaft seal and is driven by 220 HP, 1500 rpm motor (Full load amps-290 amps). Power is transmitted to pump by gearbox. Pump rotating speed is 5130 rpm. The pump rated capacity is 27 cubic meter / hour at 800 meter head total developed head (450 LPM at 830 meter head). This pump is running parallel to the pacific pump. This pump was having high noise near to pump suction nozzle in the range of 106 dba. In view of its high noise problem rectification, various studies were done. Detailed vibration and noise measurement was carried out on pump 1NDO6C and its suction line of unit#1 in all direction three directions in consultation with RED, BARC- Mumbai on 23 rd June 2005 and these data was compared with Unit#2 pump of same make. Fig. 8 Following observations were noticed: Overall vibration of suction pipeline varied between 20 to 50 mm/sec (peak) at different locations. Fig. 9

NDE 2009, December 10-12, 2009 61 Fig. 10 Fig. 11 is approximately 6-8 inches. As per pump standards the straight pipe length after bend/elbow is required to have length of 5 to 10 times pipe diameter to ensure stream line flow to pump suction. Based on above observations its was inferred that high noise and high suction pipe vibration was due two phase flow or turbulent flow which excite the piping shell mode. So, re-routing of pump suction line at the take-off point was done to minimize the possibilities of two phase flow due to its inverted U-type pipe line near to take-off point and also straight spool length between suction elbow and suction nozzle increased from 2.5 inches to 22 inches to minimize turbulence at pump suction. Same modification is shown in the Fig. 9. After above modification the sound level was measured for different flow. In normal condition sound level was found to be 102 dba. But when flow was reached to 490 dba sound level reduced to 97 dba. In Dec 2006 sound level was again measured and sound level was found to be 105 dba. For further study and analysis of same expert from RED, BARC visited TAPS on 22.01.09. Two probes were fixed on the suction side pipe flanges of 1NDO6C & 2NDO6C, to obtain real time frequency spectrum. The measured vibration signature on the suction line of both pumps was compared (refer Fig. 10). It was observed that the spectral content in the suction line of 1NDO6C had high amplitude up to 13.5 KHz. Some of the dominant peaks were 681.12 Hz, 2.775 KHz and 8.1375 KHz. These frequencies appear to be some of the higher shell modes of pipe which were excited by the flow. These shell modes can be physically felt on the piping. These responses inferred that either pump was cavitating or there was two phase flow of very high velocity. During condition monitoring of clean up pump 1NDO6-C on 08.06.07 it was found that vibration at pump out-board bearing in vertical direction (POB(V)) increased from 5.0 mm/sec to 13 mm/sec Due to increase in vibration, daily monitoring of pump 1NDO6-C performance parameter was done. Subsequently vibration signature was also taken. Vibration was in the range of 10-11 mm/sec at POB (V) till 12.06.07 and predominant vibration frequency found to be at 1 RPM. On 15.06.07 pump vibrations were again measured and maximum vibration was found to be 21mm/sec at POB (V) and 14 mm/sec at PIB (H). So, there was significant increase in vibration amplitude. Due to this vibration signature was again taken and it was found that predominate vibration frequency was at both 1 RPM and 2 RPM. Again pump performance parameter and vibration was taken for different discharge flow condition. There was no change found in vibration level. Probable causes of high vibration were either rubbing or amplification of unbalance forces due to mechanical looseness or both. This caused deterioration of pump and result in increase in vibration within a short span of time. After review it had been decided to replace the 1NDO6C pump barrel assembly with spare barrel assembly to prevent further deterioration. After old pump barrel assembly removal visual inspection was done and following observation were the made:- This pump has balancing drum, which is keyed to shaft, to balance the pump axial thrust and water from the radial clearances between balancing drum and balancing sleeve is continuously discharge to the suction line near to pump suction nozzle of pump by a ½ SS line to maintain the required pressure at balancing drum. This ½ SS line is connected to the pump suction line by thread-o-let with restricted orifice and this line joints to pump suction has erosion (Ref Fig. 12A, B, E). Balancing drum discharge line had been disconnected from the pump casing and pump suction line after observing the above erosion at its discharge end to pump suction line. Subsequently, heavy erosion was noticed in the restricted orifice. (Ref. Fig. 12 C) Balancing drum which is keyed to the pump shaft has serration that use as a pressure reducer when it is in

62 Acharya et al. : Proceedings of the National Seminar & Exhibition on Non-Destructive Evaluation Fig. 12 Fig. 13 assembled condition This serration was heavily eroded in one half. No abnormalities were noticed in the balancing drum sleeve. (Ref. Fig 12 D) There was scratch marks were found over the thrust bearing pad. Rubbing marks were found on both PIB and POB bearing metals and also scoring marks observed on pump shaft PIB journal portion. 1st stage impeller of this pump had cavitation damage at its entrance portion. There is rubbing marks also found on the shaft under suction end. Similar rubbing observed on pump suction casing throat portion. The pump barrel was replaced with spare barrel assembly and RO of balancing drum discharge line was replaced with a new fabricated RO (RO material is SS 304) having orifice size was 7mm. The size of RO was selected after measuring the restricted orifice of other pump same make pump 2NDO6C. After pump alignment to gearbox and motor the oil flow to the bearings, coupling and gearbox was adjusted as per manufacturer recommendation. Pump performance testing was done after barrel assembly and RO replacement in both uncoupled and coupled condition. In coupled condition performance parameter was taken for different pump flow condition.

NDE 2009, December 10-12, 2009 63 Following were the observations:- The pump performance parameter including sound level and vibration was measured for different flow conditions by keep other parallel connected in recirculation mode. The sound level near the pump suction flange is found to be 97 dba whereas before replacement sound level was 105 dba (This problem was persisting since many years). The pump parameters are comparable with previous commissioning data of pump. The vibration piping down stream of flow element in pump suction line is reduced to 17 mm/sec earlier its vibration was 30-50 mm/sec. (refer Fig. 13) When both pumps 1NDO6B & 1NDO6C are operated with rated flow, the performance data was collected and its performance data are acceptable. Discharge pressure- 88 kg/cm 2, Suction pressure-3.1 kg/cm2, TDH- 84.9 kg/cm 2 Flow 371 Lpm, Total system flow- 840 Lpm, Sound level near suction flange- 97 dba Maximum Vibration- 6 mm/sec at MIB (H). Pump high noise problem was solved to great extent. This high noise problem was due to flow perturbation in the pump suction which resulted in the cavitation of 1st stage impeller at its entrance. This perturbation was caused by high pressure water entry in the pump suction due to erosion of balancing drum serration which was due to increase in radial clearances between balancing drum and balancing sleeve. This caused high flow in the balancing drum relieving line going to pump suction. Erosion of restricted orifice and its joint to suction line was due to high pressure differential and high flow across RO. When this high pressure water mixed with low pressure suction water than it generate pressure pulses which excite the piping shell mode and resulted in high noise. 6. Conclusion Systematic vibration signature analysis has assisted in solving the above specific cases of high vibration. So, vibration signature analysis is very important diagnostic tool for reliability centered maintenance. References 1. GE power system: Generator rotor thermal sensitivity-theory and experiences GE-3809 2. Reliability-centered maintenance 2nd edition by John Moubray 3. Report no RED/VLS/3013/2005 dated 08.08.05 by Mr A Ramarao, RED, BARC 4. TAPS report no perf/ts/229 dated 25.01.09 5. Pump Hand Book by Igor J. Karassik, Joseph P. Messina, Paul Cooper, Charles C. Heald