SARNIA ~t 5,2003 ECT~O by, Eduardo ~ustamante
~ GTtlD5 ScheduJed for a Co inspection on Se~tembe~ 2003 - Plant Name: Dow- Sarnia Customer: GT Type: EOH" TransAIta (Oct. 2002, previous Dow Chemical) 11 D5 - Outdoor unit, installed in 1977 204,000 h approx. (09/03) - Starts: 550 approx. ( 90 since 2000) Last C inspection: October, 2000. Previous inspection on (all blades and vanes were replaced) 1997 - Last A inspection July, 2001 (Alstom) ALSTOM Power ALSTOM Power inc. 2002 We reserve the rights in this document and the information contained therein. Reproduction, use or disclosure to third parties without expressed written authority is strictjy forbidden. Slide 2
TechnicaB issues - Unit has been running at firing temp of about 1800-1810Fo - High TAT spread reported just prior to last A inspection ( 07/01)o Could result in potential high fallout rates for stationary components. - Customer has established their own profile for TAT probes, TAT survey and Performance test recommended before C inspection, - Balancing performed in 01/01 to reduce high vibration at operating speed. - Turbine Blades row 5 are laced. 11DM upgrade option would eliminate this requirement. ALSTOM Power ALSTOM Power inc. 2002 We reserve the rights in this document and the information contained therein. Slide 3 Reproduction, use or disclosure to third parties without expressed written authority is strictly forbidden.
Technica~ issues - Wear and tear reported in Inspection reports within our experience. - Installed blades have minor TBC loss on leading edge and back side. Light to moderate rubbing on tips of all row 3 blades. - Reconditioning risk on row 3 blades due to tip thinning issc~eso - Review of Rotor operational history and site phased array inspection are required. - EM Generator appears to have room for power increase 1 idm option) since its operating output is significantly below rating ( 58 MW vso 72 MW).Option to provide Generator diagnostic service during C inspection. - Tricen control system. Option to upgrade controls to ALSTOM P320 with new lntellution - Burner installed in 1988 is of Coen design, rebuilt in 200t ALSTOM Power ALSTONI Power inc. 2002 We reserve the rights in this document and the information contained therein. Slide 4 Reproduction, use or disclosure to third parties without expressed written authority is strictly forbidden.
ALSTOM Power ALSTOM Power Inc. 2002 We reserve the rights in this document and the information contained therein. Slide 5 Reproduction, use or disclosure to third parties without expressed written authority is strictly forbidden.
11 C ritic a ~ a c tiv itie s D u ra tio n A c Co days Duratio~ PHASE 1 Shut down of G T Pre inspection alignment readi D ism antling of G T De- blading work PHASE 2 Blading work Combustor & U-duct fit up R eassem bling of G T R e- Aiignm ent Hot Commissioning of GT Balancing 1 1 3 4 9 13 3 16 10 26 7 33 14 47 3 5O 3 53 1 54 ALSTOM Power ALSTOIVl Power inc. 2002 We reserve the rights in this document and the information contained therein. Slide 6 Reproduction, use or disclosure to third parties without expressed written authority is strictly forbidden.
KVA ~ENER~YFO!~ RATING AC A/ ~ERES VOLTAGE HYDROGE! I-- COOLED SY,.[CI[tloIqous Gi~NEIOV~Oll DOW CIIEI4ICAL OF CANADA, LTD SA[~qIA ~ OI.~TAN.IO Serial i~umber 175870005,5 psi Z H 2 68,000 2,726 14,400 15 psig H 2 78,200 3,135 14,400 COOLING ETHYLENE GLYCOL SOLUTION 30 psig H. 2 85,000 3,408 14,400 Generator coolers (2): 440 GPM total solution flow at 790F max inlet tempo.125 psig operating, i0.0 psid pressure drop Exciter cooler (i): 20 GPM solution flow at 79 F max. inlet temp. 125 psig operating, 6 psid pressure drop GAS VOL~.~E The static gas volume of the generator is 1300 cubic feet. ~ DICHINE CONSTANTS* Rated current, direct axis synchronous reactance (Xdi) 207% Rated current, direct axis transient readtance (X di) 30% Rated voltage, direct axis transient reactance (X dv) 26% Rated voltage, direct axis subtransient reactance (X"dv) 16% Rated voltage, negative sequence reactance (X2v) 16% Rated voltage, zero sequence reactance (XOv) 8% Direct axis, open circuit transient time constant (T do) 7 4 seco Direct axis, short circuit transient time constant (T d).9 seco Direct axis, short circuit subtransient time constant (T"d) ~04 SeCo Armature time constant (Ta) 0.3 sec. Ac seal oil pump motor Dc seal oil pump motor Vapor extractor motor (loop seal) Gas dryer blo~er motor Purity meter blower motor AUXILIARY EOUIPMENT RATING ~2 hp, 600 Vac, 1150 rpm, 3-phase 2 hp, 120 Vdc, 1150 rpm 2 hp, 600 Vac, 3450 rpm, 3-phase 1/3 hp, 115/230 V, 3450 rpm, i-phase 115 V, 1-phase Total weight: 300,000 pounds Rotor weight: 43,300 pounds (including exciter) Rotation:. clockwise facing end opposite turbine Bearing journal dis.: 12 inches nominal Bearing clearance:.027 to 030 inch horizontal (on dia. as mfd.).015 to.018 inch vertical Hydrogen-side seal clearance:.001 to.004 inch horizontal (on dis, as mfd.) 007 to o011 inch vertical Air-side seal clearance:.004 to 007 inch horizontal (on dia. as mfd.).013 to 018 inch vertical " Hydrogen-side seal oil drain f].o~: approx, io0 GP~f total Differential bet~een seal-oil and generator hydrogen pressure: 5 psid *At 85,000 kva and 83].5 volts per phase. 1-5 11/76
Electric Machinery Mfg. Company, Minneapolis, Minn. U.S.A.
From: CCSTAR::BAJC "Peter Bajc Energy Systems 5085" 24-AUG-1995 11:30:29.23 To: EASTMAN CC: Subj: For your information and manuals too \! ~ this list together for the tech centre and thought that you may be interested in keeping a record of the retaining ring material. Sarnia Site generator retaining ring material. Machine Manufact. Rating P.F. Volts Mat l Cooling GT831 @E 64 mva.85 14,400 18n~ 5cr H2 GT841 GE 64 mva.85 14,400 18mn 5cr H2 GT851 Elec. Machinery 85 mva.85 14,400 ASTM 288 Class B H2 TG811 Westinghouse 33.8 mva.85 14,400 ASTM A288 5 or 8 H2 TG821 Westinghouse 33.8 mva.85 14,400 ASTM A288 5 or 8 H2 Peter
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ABB TURBINE POWER DIVISION 5309 COMMONWEALTH CENTRE PARKWAY MIDLOTHIAN, VA 23112 DATE: 6/17/93 PAGE I of 1 To: Paul Eastman Fax/Phone #: 519.339.3321 (F) 519.339.5233 (P) Company. Dow Chemical Location: Sarnia, Ontario From: Edward Spyhalskl Fax/Phone #: 804.763.2038 (F) 804.763.2018 (P) Departmenz: Gas Turbine Service and Parts Reference #: EJS-93-84 DWS-38a SUBJECT: Rotor Mass Moment of Inertia You requested mass moment of inertia values in a June 9 fax to Roll S~hmid, This is the information 1 have found; GT rotor assembly with blades and Intermediate shaft 140,100 Ib ft 2 (5905 kg m 2) Generator rotor assembly 38,600 Ib ft 2 (1625 kg m 2) Combined assembly 178,700 Ib ft 2 (7530 kg m 2) Call if you have questions. Regards, Edward Spyhalski Service Engineer