Contents 1) Vibration situation for CGC Large Steam Turbine 2) Root cause analysis and evaluation method 3) Countermeasure with result

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Preface A Large Steam Turbine had been in operation for several years and this turbine experienced the wear damage of governor linkage. Then, measured the vibration velocity profile on Governor side pedestal to identify the excited vibration mode and frequency. According to collected data, investigated the possible root causes and conducted 3D vibration response analysis to the existing and the improved pedestal. And, improved pedestal was supplied to the client and applied for actual machine during turnaround. And, finally, the advantage of new improved pedestal was confirmed. This case study introduces the typical phenomena, RCA investigation, detail vibration analysis, countermeasures and verification results as technical process. Contents 1) Vibration situation for CGC Large Steam Turbine 2) Root cause analysis and evaluation method 3) Countermeasure with result

1. Specification of Steam turbine with Gov, side pedestal TTV(Steam inlet) HP/LP casing E/H actuator HP Casing Pilot valve BRG pedestal BRG pedestal cover Base plate Section drawing of turbine Rotor BRG pedestal Turbine specification ; Max, power ; 60MW Speed ; 2830 3845 rpm Plant start ; from 2002 Contact / Slide surface BRG pedestal Casing support Gov, side brg, pedestal with cover, linkage assembly Major specification of bearing pedestal with cover assembly; 1) Fabricated welding structure 2) Separated fabricating casing support 3) Material is Carbon steel (Eq, ASTM A36)

2.1 Background Historical events at field ; Turbine start up in 2002 Gov, side pedestal Vibration increase from around 2005 Vibration up to 20 mm/s in 2012 by turbine load/speed up Vibration causes linkage lever wear and required control limit Y3 X1 X2 Y6 X3 Vibration [mm/s] (0-P) X1 X2 X3 Z1 Y6 Z1 10/Sep,/05 15/Jan,/08 30/Apr,/08 20/Mar,/11 24/Jan,/12 Site measurement points (View from Gov, side) Pedestal vibration record from 2005 to 2012

2.2 Background Steam flow map F B LEVER F B LEVER GV linkage damage condition Roller Operation condition ; It was shifted actual inlet steam flow against E/H actuator signal. Occurred Impossible control area. Inlet Steam flow Impossible control area Rotating speed

2.3 Background Site vibration measurement record ; Velocity in mm/s Bump test result of pedestal Power cylinder E/H actuator Exh,side Pedestal The out-of-phase mode Casing support Original position Pedestal Site measurement points (No,30) Casing support Measured vibration mode at 3555 rpm (59Hz) The main characteristic of the vibration mode is an out-of phase (counter-motion) mode between main pedestal and casing support Measured vibration mode under operation (View from Exh, side)

3. Root Cause Analysis for Bearing Pedestal Vibration Root cause failure analysis found on 3 main items as below; 1, Excessive external force 2, Increase of modal mass on bearing pedestal 3, Decrease of dynamic stiffness Foundation degradation Bearing pedestal stiffness Natural frequency excitation Resonance with rotating speed

4.1 Response analysis of 3D Full modeling In order to clarify the vibration mechanism, it performed vibration 3D response analysis(cod-nastran) with current bearing pedestal. 3D full FEM modeling Rotor modeling with exciting force Mass data with Boundary condition Dynamic vibration response analysis Original pedestal New pedestal

4.2 Response analysis of 3D Full modeling Rotor modeling with excitation force calculation Step-1 : Calculate BRG reaction force (F) Step-2 : Analysis Vibration response

5.1 Analysis result of original pedestal in hot condition View from TOP Comparison between Measurement data and Analysis result by animation mode. View from 3D Result 3D response analysis method is almost suitable for site operating condition. Confirm the out-of-phase(counter-motion) mode between main pedestal and upper casing support, and moving up for pedestal contact surface. View from front side View from side This vibration main cause is the decrease of pedestal stiffness Analysis vibration mode result Measured vibration mode at site (View from Exh, side)

5.2 Analysis result of original pedestal in hot condition Final analysis results of fabricated pedestal type X3 Result Natural frequency 61.8Hz is in to the turbine operating speed range at hot condition, it shifted from cold condition. Vibration level in analysis is 10 to 30mm/s 0-P around normal to max speed as same as site vibration level. Equivalent to full contact area of pedestal to be reduced. Contact surface 61.8 Hz 73 Hz(Cold) Operation range ; 48.8 64.0 Hz Full contact blue colored only View from pedestal lower side

6. Comparison of original and improved pedestals Requirement for new pedestal design 1) Full contact condition of pedestal surface. 2) Rigidly connection between pedestal body and casing support without freestanding. Old fabricated type New casting type Casting pedestal type has more high stiffness than original type

7.1 3D analysis result of improved pedestal in hot condition Final analysis results of Casting pedestal type X3 Result a) Natural frequency 40.7Hz to be out of operation range, and satisfied with API standard (less than 41Hz). b) Vibration level in operation to be much lower at 0.3 to 1 mm/s 0-P even by 5-times of API unbalanced limit Contact surface Original(hot) 40.7 Hz Operation range ; 48.8 64.0 Hz

7.2 3D analysis result of improved pedestal in hot condition Following shows vibration mode of animation for original and improved pedestal. New casting pedestal has a big advantage against original pedestal Original pedestal Improved pedestal

8. Site verification result for permanent solution Result for applying of new improved pedestal Governing valve Vibration [mm/s] (0-P) 20 18 16 14 12 10 8 24 Jan 12 3505rpm 6 Apr 13 3540rpm E/H actuator with linkage Improved pedestal with cover 6 4 2 0 X1 X2 X3 Y3 Z1 Y6 Vibration record improved pedestal in 2013 Out view of similar turbine Result ; Vibration level in rotating speed to be much reduced to less than 3.0 mm /sec (0-P), which means reduction of 80% compared with the existing pedestal vibration level.

9. Conclusion 1) Summary of analysis result Pedestal Analyzed N F Vibration level in operation Note Fabricated type (Original design) 61.8Hz (Hot condition) Maximum 30mm/s 0-P (H-direction) Almost same as site bump test (73Hz) with cold condition 69.2Hz. Casting type (Improved design) 40.7Hz Less than 1mm/s 0-P (H-direction) 17% separation margin against 48.8Hz (Min. speed) satisfied with API standard of more than 16% 2) 3D response analysis was carried out using field measurement data. - Analysis was confirmed root cause of site pedestal vibration. - Analysis model used to design new bearing pedestal, and confirmed the expected vibration include separation margin. - Improved bearing pedestal retrofit to similar machines. - Field record verified the improved vibration response analysis.

10. Lessons Learned Requirement items to future structure design. - The robust design that can applicable a wide operation speed range. - The high stiffness design include separation margin based on API. - Utilize full 3D analysis based on actual structure modeling with loading data, and establishment of guidelines. Sample ; Design check sheet for Dynamic response analysis Operation range with margin Vibration (p-p) (μm Allowable vibration line Safety zone Should be applied the Turbine structure design. Operation speed Hz

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