Combustion Turbine Outages For 2008

Similar documents
CCHMP Comments on ConocoPhillips Incident Report For 10/22/10 Flaring Event

Modulating Furnace Information. Warning on Meter Setting - Read First!

ATA 49 AUXILIARY POWER UNIT

This chapter contains information on DC Generation, External Power, and Electrical Load Distribution.

CENTRIFUGAL CHILLER. Lubrication System Pull oil sample for spectroscopic analysis.

ELECTRICAL HAZARD EXAMPLES

DASSAULT AVIATION Proprietary Data

B-03 ELECTRICIAN TRAINING SKILL DEVELOPMENT GUIDE

24-00 ELECTRICAL POWER

Standby Power Systems

PLANT HATCH FEEDWATER SYSTEM OPERATING EXPERIENCE. Significant events from 2015

TABLE OF CONTENTS. Understanding the Troubleshooting Instructions...2 Signal Light...2 Harness Connections...2 Inspection...2

Application Note. Case study Early fault detection of unique pump bearing faults at a major US refinery

Appendix C. Interval Every 2 Year. Functional Test Weekly Monthly Quarterly. Semi. Every 3. Engineering Studies

DG SYNCHRONIZING &AMF PANEL

E Series CE Approved Intermittent Pilot Ignition Control

Clay McClinton Rotating Equipment Reliability Analyst, Chevron. Dan Phillips Manager Global Field Services, Kop-Flex

POWER SYSTEM OPERATING INCIDENT REPORT TRIP OF 220 KV C BUSBAR AT GORDON POWER STATION ON 26 NOVEMBER 2011

POWER SYSTEM OPERATING INCIDENT REPORT TRIPS OF YALLOURN W POWER STATION UNITS W1 AND W3 ON 14 NOVEMBER 2012

ALTERNATOR STARTUP Turning gear to full operation. Procedure initiated by:. 7/03 Before starting procedure, remove all check marks.

Programmable Safety Systems for Burner Management on Gas Turbines.

Health and Safety Executive, Technology and Health Sciences Division, Magdalen House, Bootle.

BLOWER VACUUM SWITCH FAILED OPEN

WS2H/ WS3 Error Codes

Case Study on On EHV Circuit Breaker Flashover NTPC-SINGRAULI

GUIDE TO MAINTENANCE PRACTICES FOR DISTRIBUTION NETWORKS IN THE DISTRIBUTION SECTOR OF THE NAMIBIAN ELECTRICITY SUPPLY INDUSTRY

Solid Dielectric, Triple Option Reclosers Catalog O-vlt14

LESSONS LEARNED FORSMARK EVENT Presented To IEEEE

Solid Dielectric, Triple Option Reclosers Catalog O-vlt14

Tattletale Annunciators and Magnetic Switches

Centro América Application of EMI Diagnostics to Diesel Generators

TECHNICAL SERVICE DEPARTMENT Technical Service Bulletin LowNOx Commercial Gas Electronic Spark Ignition Sequence

Application Note. First trip test. A circuit breaker spends most of its lifetime conducting current without any

BIGLA30-T/BIELA14-T Event Codes Quick Reference EXPLANATION CORRECTIVE ACTION PARTS TO CARRY ON SERVICE CALL

OVERLOAD PROTECTION. All electrical circuits must have some means of protecting against overload.

TABLE OF CONTENTS. Understanding the Troubleshooting Instructions...2 Signal Light...2 Harness Connections...2 Inspection...2

Solid Dielectric, Single Phase Recloser

Bombardier Challenger Auxiliary Power Unit

BOILER PM & INSPECTION

Customer Open Date Hours Work Order Notes /9/2018 0:

Appendix B6 Gas Turbine Unit Cause Codes

ANZSASI 2000 CHRISTCHURCH ENGINEERING ANALYSIS. Vlas Otevrel

H.S. MACHINERY RING COMPRESSORS

ECU-02 Ver2.1 Automatic Engine Control Unit Operators Manual

16kA Solid Dielectric, Triple Option Reclosers Catalog VLT12

ZIP Economizer Fault Detection and Diagnostics (FDD) Table

POWER SYSTEM OPERATING INCIDENT REPORT SIMULTANEOUS TRIP OF 5A6 MT PIPER BANNABY 500 KV LINE AND MT PIPER NO. 2 UNIT ON 9 FEBRUARY 2012

DewPoint 6110 Troubleshooting Guide

Improving Plant Operations. Retrofit of Waste-to-Energy Stoker Controls to Improve Combustion and Availability

Time delay relays. The following is a timing diagram of this relay contact's operation:

Substation inspection guidelines Mark B. Goff, P.E.

INVESTIGATION REPORT PREPARED FOR: UNIVERSITY OF NORTHERN IOWA CEDAR FALLS, IA

POWER SYSTEM INCIDENT REPORT: TRIP OF NO 1 AND 2 NEW OSBORNE 66 KV BUSBARS ON 26 SEPTEMBER 2010

Technical Service Bulletin IOX/DCX Transmitter Maintenance Schedule

DEEP SEA ELECTRONICS PLC

COLDWATER LAKE FACILITIES DUPLEX PUMP STATION

PRAIRIE MINES AND ROYALTIES PAINTEARTH MINE MARION 8200 DRAGLINE ELECTRICAL UPGRADES

Synchronous motor control. 8/15/2007 Powerflow Technologies Inc 1

Web/SNMP Management Card Event Support Chart

ANDERSON, ECKSTEIN AND WESTRICK, INC.

Dual Power. Protection. Protection

team master medium voltage solid state starters

INTERCONNECTION STANDARDS FOR PARALLEL OPERATION OF SMALL-SIZE GENERATING FACILITIES KILOWATTS IN THE STATE OF NEW JERSEY

KD LV Motor Protection Relay

Start Up Instructions for the Kiln, Page 1 of 2

PROBLEM SOLVING GUIDE ELMECO SLUSH MACHINE MODEL FCM

CONTROLS UPGRADE CASE STUDY FOR A COAL-FIRED BOILER

PROTECTION OF THREE PHASE INDUCTION MOTOR AGAINST VARIOUS ABNORMAL CONDITIONS

Hayward error codes and troubleshooting

Heating and Gas Installations - December 2014

KEYLESS ENTRY SYSTEM & TIRE PRESSURE MONITOR ACCESSORIES & EQUIPMENT General Motors Corp. - Remote Keyless Entry System

NYISO Tariffs. New York Independent System Operator, Inc. Document Generated On: 2/27/2013

Evaluation of a Gearbox s High-Temperature Trip

ISO Rules Part 500 Facilities Division 502 Technical Requirements Section Interconnected Electric System Protection Requirements

FUNCTIONAL SAFETY SOLUTIONS in Solenoid Valves

PPL Gas Insulated Substations: Design Considerations and Lessons Learned. Nicholas Matone Support Engineer, T&S Standards

INSTALLATION AND SERVICE INSTRUCTIONS AND REPAIR PARTS LIST FOR MODELS K4RP & K4VP SUBMERSIBLE SOLIDS-HANDLING SEWAGE PUMPS

MODEL 520 REMOTE START ENGINE MANAGEMENT SYSTEM

Electromagnetic Industries LLP

5220 AUTOMATIC MAINS FAILURE MODULE OPERATING MANUAL

POWER GENERATION SYSTEMS

Equipment Strategy for Stand By Diesel Generators Strategy

Safety Design of CHAdeMO Quick Charging System

Advantage-D. Operating Instructions and Maintenance Manual. Central Vacuum Systems (Expandable/Modular Models) (Ver.

MODEL 233P/111P/233P-1.5

HT Dielectric Withstand Tester Volts AC Output 25mA Leakage Option

MANDATORY SERVICE BULLETIN NO. MSB /1

FABER BURNER ROUTINE MAINTENANCE

Battery Control Center - Diesel

VAGABOND S HANDBOOK TRANSMISSION

The behavior of the cycloconverter fed gearless drive under abnormal electrical conditions

AUTOMATIC FOODSERVICE EQUIPMENT. AUTOMATIC ELECTRIC BROILER MODELS 824E & 850E and 624E & 650E. B-Series Broiler OWNER S MANUAL

Quick Start Guide TS 910

TIME REQUIREMENT GUIDE (TRG)

P445 Series Electronic Lube Oil Control

BRIVIS DUCTED INVERTER SERVICE MANUAL DRCi

Grounding Of Standby & Emergency Power Systems

MANUAL ELECTRIC FIRE PUMP CONTROLLERS METRON SERIES M450

INSTALLATION AND OPERATION MANUAL ARM-4073 AUTOMATIC REPRESSURE MODULES

Cutler-Hammer. Instructions for Installation, Operation, and Maintenance of the AMPGARD Reduced Voltage Soft Starter

Transcription:

OCKET E 09-091 EXHIBIT - MC-7 Combustion Turbine Outages For 2008 The following outages took place at PSNH's combustion turbine units during 2008: Lost Nation CT-l Major work that was completed at Lost Nation during 2008 included the installation of high capacity emergency vents on the two fuel storage tanks to comply with the latest fire standards and the installation ofoil leak detectors to comply with environmental regulations. Lost Nation - 1 4/14-4.33 days performed were a visual inspection, general cleaning, and annual equipment tests and servicing the diesel starter engine. Testing and inspections revealed no abnormalities. White Lake CT-l Major work that was completed at White Lake during 2008 included the installation of high capacity emergency vents on the four fuel storage tanks to comply with the latest fire standards and the installation of oil leak detectors to comply with environmental regulations. White Lake-l 3/11-0.31 days The E-SCC dispatcher received an alarm that the unit failed to start while the unit was not in operation or under request to do so. The unit had a new controller installed in October 2007 along with other control changes. The Ethernet module in the new Programmable Logic Controller (PLC) was found to be defective and bypassed so the unit could be returned to service on a remote basis. The module was replaced on 3/14. B 4/28-4.00 days performed were a visual inspection, general cleaning, and annual equipment tests. Testing and inspections revealed no abnormalities. 85

C 6/2-0.32 days in operation or under request to do so. The module position switch (detects loose logic cards) in the new PLC was found to be defective and replaced. The unit was returned to service. 6/13-0.09 days in operation or under request to do so. The system computer was found in the offposition and would not restart. The operator unplugged and plugged the computer back in resulting in a successful reboot. The unit was returned to service. Subsequent investigation warranted the installation of an Uninterrupted Power Supply which was installed on 7/29. The UPS installation seems to have corrected the problem. E 7/18-0.13 days in operation or under request to do so. Thunderstonns in the area caused a vibration alann that initiated the alann. lanns were cleared and the unit was returned to service. The vibration monitor was scheduled to be calibrated on 7/30. F 7/24-0.07 days in operation or under request to do so. Thunderstorms in the area caused a vibration alann that initiated the alann. lanns were cleared and the unit was returned to service. On 7/30, the vibration monitor was calibrated and reconfigured so that it would be in the off position when the unit was not in operation and turned on when the start command is given. G 9/26-0.15 days in operation or under request to do so. The operator found the generator breaker tripped and a generator high temperature alann. The operator removed and reinstalled the generator trip circuit card in the annunciator panel (not part of the new controller) which successfully reset the alann. The unit was returned to service. Subsequent testing of the generator trip relay, remote temperature devices, and wiring found no abnormalities. 86

Schiller CT-l 1/17-0.3 days The unit failed to start when called on by the ISO. Low air pressure maxed out the pressure speed timer. The air compressor was undergoing repairs in Germany and air pressure was taken from Schiller Station to start the unit. To increase efficiencies and reduce losses, the air pressure at Schiller was reduced to 250# from 500# which is insufficient to start the unit. The time/speed setting was increased to allow more time to bring the unit up to required speed before alarming. PSNH has set up an evaluation team to evaluate this unit including maintenance practices and problems occurring at this unit. PSNH notes that the recommendations were implemented in 2009. B 3/3-1.4 days The unit was scheduled for its arumal inspection with ISO-NE starting 3/8 (effectively 3/1 0 for normal work days). The unit was mistakenly taken out of service a week early while Schiller Station was in an outage for Unit #5. While reassembling the unit, the replacement of a damaged igniter extended the outage. The igniter was damaged during reassembly of the unit when a shroud for the hot side of the burner cans was slid back over the igniter section of the combustion turbine to allow accesses to the burners cans. The exciters are somewhat delicate and located in close proximity to the shrouds. This type of damage has not been common over the almost 40 year life of the unit. Liberty views this incident as accidental. Once reassembled, the unit was returned to service. To prevent reoccurrence of taking the unit out on the wrong date, PSNH reviewed week beginning and week ending calendars as used by the ISO with maintenance personnel. C 3/1 0-4.5 days perfonned were a visual inspection, general cleaning, and annual equipment tests. Testing and inspections revealed no abnonnalities. 6/5-0.1 days While in standby mode, an alarm for high generator stator temperature was received. Investigation found the trip relay in the trip position. The relay was cleaned and tested and the unit was returned to service. new relay was ordered to replace the exiting relay at an appropriate time in the future. E 6/20-0.0 days While in standby mode, an alarm for high generator stator temperature was received. Investigation found the trip relay in the trip position. This is an identical outage cause as discussed in Outage above. The new relay ordered as a result of Outage above was 87

received on 6/17 and there was insufficient time since receiving the relay for it to be installed prior to this outage. The new relay was installed at this time. F 9/28-0.1 days While in standby mode and cormected to the 34.5 kv system (The Schiller CT has the capability to feed into the 34.5 kv system or to Schiller Station), a lightning arrestor just outside the coal pile on the 367 34.5 kv line failed. The failed lightning arrestor was isolated, the unit was switched to its alternate feed, and the unit was returned to service. G 10/20-0.1 days The unit was called to operate by the ISO and went to full load. fter approximately 5 minutes, a vibration alarm for probe #3 shut the unit down. Investigation found that one of the vibration probes was dirty. The probe was cleaned and the unit was returned to service. PSNH notes that all probes were inspected and cleaned in the 2009 armual inspection. H 10/28-0.0 days This was a short scheduled outage to replace a thermocouple monitoring temperature of the turbine. Two turbine temperature alarms were received the previous day and identified the need for replacement. MerrimackCT-1 Major work completed at the Merrimack combustion turbine included the removal and replacement of the free (rotating blade) turbine on CT-l. CT-1 and CT-2 are cormected to the 115 kv transmission yard via a common step transformer and have common fuel systems. Some of the concurrent outages listed below are a result of those configurations. 4/21-4.3 days This scheduled outage was taken to perform the armual inspection. Included in the work performed were a visual inspection, general cleaning, and annual equipment tests. Testing and inspections revealed no abnormalities. uring this inspection, the free turbine (rotating blade) was replaced with a loaner so the PSNH turbine could be refurbished. Once refurbished, the PSNH turbine would be reinstalled (See Outage l-e below) lthough not required to because of configuration, the CT-2 annual outage was performed at the same time. (lso see Outage 2- below) 88

B 5/7-0.2 days This outage was taken to replace a "T" in the CT-1 fuel line. The "T" was replaced and the unit was returned to service. fuel filter leak on CT-2 was also repaired during this outage. (lso see Outage 2-B below)the fuel system consists of common fuel tanks with a common feed line and a common filter. The fuel system then splits into two lines with a separate filter for each unit. C 5/1 0-0.2 days This outage was taken to repair a lube oil pump leak. The leak was repaired and the unit was returned to service. 7/21-1.0 days While in operation, a high vibration initiated a unit trip. The turbine vendor did a boroscope examination of the area surrounding the vibration location for damage. No damage was found. The vibration probe was replaced and the unit started without incident. E 10/6-4.1 days This scheduled outage was taken to reinstall the PSNH free turbine so that the loaner turbine could be returned. (lso see Outage I- above) F 10/26-0.1 days uring the Merrimack-l overhaul, the CT-1 circuit breaker was replaced. It was required to de-energize the bus to test this breaker. (lso see Outage 2- below) Merrimack CT-2 lis - 1.4 days performed were a visual inspection, general cleaning, and annual equipment tests. Testing and inspections revealed no abnormalities. This outage was done in conjunction with Outage I- above. 89

B 5/7-0.2 days This outage was taken to repair a fuel filter leak on CT-2 and was done in conjunction with a fuel line repair to CT-1. The leak was repaired and the unit was returned to service. (lso see Outage I-B above) C 10/20-1.0 days The unit was called upon to run by the ISO. CT-2 failed to phase to the system. Bad diodes were found in the dead bus relay board. The relay board was replaced and the unit was returned to service. 10126-0.1 days This outage was required so that the bus could be de-energized for testing of the new generator breaker on CT-1 because of the step transformer configuration. (lso see Outage 1-F above) Evaluation Except for Outages Schiller CT-I and B Liberty reviewed the outages above and found them either to be reasonable and not unexpected for these units and their vintage, or necessary for proper operation of the unit. Liberty concluded that PSNH conducted proper management oversight. Schiller CT-I Outages and B Schiller CT-I, Outage I- This outage is for identical reasons as the outage described in the review of the 2007 SCRC (Outage H on 12/13). Liberty recommends that the replacement power relative to this outage be disallowed. The decision to reduce air pressure at Schiller either had no review or a review at such a level that the combustion turbine was not considered. Even a cursory review should have raised the question of adequate air pressure for starting the combustion turbine. Schiller CT-l, Outage I-B The time for the outage and outage extension were 0.65 days and 0.78 days respectively. Liberty recommends that the replacement power relative to the early removal of the unit (0.65 days) be disallowed. Removal of the unit was not adequately communicated especially when the well established intent of outage scheduling at Schiller is to sequence unit outages for work force purposes. Operators should have known outage schedules and unit scheduling requirements. 90