Sub Regional RTEP Committee - Western. October 21, 2009

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Transcription:

Sub Regional RTEP Committee - Western October 21, 2009

Dayton Transmission Zone N-1-1 Thermal Violation Sidney - Shelby 138 kv line for the loss of Darby 138/69 kv transformer and Urbana 138/69 kv transformer Reconductor E.Sidney - Shelby 138 kv Estimated Project Cost: $0.532 M 2

N-1-1 Thermal Violation Greene - Alpha 138 kv line for the loss of Greene 345/138 transformer 1 and Greene 345/138 kv transformer 2 Reconductor Greene - Alpha 138 kv Estimated Project Cost: $1.63 M Dayton Transmission Zone 3

N-1-1 Thermal violation Bath - Trebein 138 kv line for the loss of Bath - Miami 345 kv line and Bath 345/138 kv transformer Perform sag study on Bath - Trebein 138 kv line to ensure clearance for rating increase Estimated Project Cost: $0.0 M Dayton Transmission Zone 4

Duquene Transmission Zone N-1-1 thermal violation Arsenal - Highland 138 kv line for the loss of Logans Ferry 345/138 kv transformer and loss of 580 MW unit at Cheswick Restudy rating of Arsenal Highland 138 kv underground d line Estimated Project Cost: $0.0 M 5

N-1-1 voltage violation Voltage violations at Progress Park and Wythe stations for the loss of Adkins - Broadford 138 kv circuit and Huffman - Jacksons Ferry 138 kv circuit Add 28.8 Mvar 138 kv capacitor bank at Huffman and 43.2 Mvar 138 kv Bank at Jubal Early and 52.8 Mvar 138 kv Bank at Progress Park Stations Estimated Cost: $2.4 M AEP Transmission Zone 6

N-1-1 1 Voltage violations Voltage violations at Sullivan, Gardens, Reedy Creek, Short Hills, and Holston Stations for the loss of Nagle - Reedy Creek 138 kv circuit and Boone Dam- Holston 138 kv circuit it Add 28.8 Mvar 138 kv capacitor bank at Sullivan Gardens and 52.8 Mvar 138 kv Bank at Reedy Creek Stations Estimated Cost: $2 M AEP Transmission Zone 7

N-1-1 1 voltage violations Low voltage violations in Beaver Creek, Morgan Fork, and Johns Creek areas for the loss of Beaver Creek - Morgan Fork and Beaver Creek - Johns Creek 138 kv Circuitsit Add a 43.2 MVAR capacitor bank at the Morgan Fork 138 kv Station Estimated Cost: $0.8 M AEP Transmission Zone 8

AEP Transmission Zone N-1-1 voltage violation Low voltage violations at Darrah, North Proctorville, Tristate West, and Huntington areas for the loss of Darrah - North Proctorville and Tristate - West Huntington 138 kv Circuits Add a 64.8 MVAR capacitor bank at the West Huntington 138 kv Station Estimated Cost: $0.8 M 9

Dayton Transmission Zone N-1-1 voltage violation Low Voltage magnitude violation at Shelby 138 kv for the loss of the Shelby 345/138 kv transformer + losses of Eldean - Staunton Tap 138 kv line and Staunton Tap Miami 138 kv line Add 2 nd 345/138 kv transformer at Shelby (B1062) Estimated Project Cost: $7 M 10

Dayton Transmission Zone N-1-1 voltage violation Low Voltage magnitude violation at Sidney 138 kv for the loss of the Shelby 345/138 kv transformer + losses of Eldean - Staunton Tap 138 kv line and Staunton Tap Miami 138 kv line Add two 30 MVAR capacitor banks at Sidney 69 kv station (B1063) Estimated Project Cost: $0.6 M 11

Dayton Transmission Zone N-1-1 voltage violation Low Voltage magnitude violation at Eldean 138 kv for the loss of the Shelby 345/138 kv transformer + losses of Eldean - Staunton Tap 138 kv line and Staunton Tap Miami 138 kv line Add a 30 MVAR capacitor bank at Eldean 69 kv station (B1064) Estimated Project Cost: $0.4 M 12

Dayton Transmission Zone N-1-1 voltage violation Low Voltage magnitude violation at Blue Jacket 138 kv for the loss of the Darby 138/69 kv transformer + losses of Quincy E. Sidney 138 kv line, E. Sidney Shelby 138 kv line, and Quincy Logan 138 kv line Install a new Shelby 138/69 kv transformer at Shelby station (B1065.1) Install a 69 kv line between Shelby 69kV station and Blue Jacket 69 kv station (B1065.2) Install a new 30 MVAR capacitor bank at Blue Jacket 69 kv station (B1065.3) Estimated Project Cost: $12.9 M 13

Dayton Transmission Zone N-1-1 voltage violation Low Voltage magnitude violation at Amsterdam 138 kv for the loss of Southwest Lima Shawnee Road 138 kv line and Shawnee Road Lima Ordnance Junction 138 kv line + losses of Southwest Lima West Moulton 138 kv line o Install a new 30 MVAR shunt at Amsterdam 69 kv station (B1066) Estimated Project Cost: $0.4 M 14

Dayton Transmission Zone Voltage drop violation at Logan 138 kv station for the loss of the Darby 138/69 kv transformer + loss of Urbana 138/69 kv transformer Install a new 30 MVAR shunt at Logan 69 kv station (B1067) Estimated Project Cost: $0.4 M 15

Dayton Transmission Zone N-1-1 voltage violation Voltage drop violation at Darby 138 kv station for the loss of Centerburg Conesville 138 kv line + loss of Hyatt Delaware 138 kv line Install a new 30 MVAR shunt at Darby 69 kv station (B1068) Estimated Project Cost: $0.4 M 16

AEP Transmission Zone Supplemental Project Bayer Corporation (Newark Compounding Facility) has requested 69 kv service to their facility in Newark, Ohio. The service can be provided by installing, removing and relocating 69 kv lines in the Newark Ohio Industrial Park. Estimated Cost: $0.972 M (Approximately $0.555 M plus tax gross-up will be reimbursed by the customer) Expected IS Date: 7/15/2010 17

Duquesne Transmission Zone Supplemental Project Add third Crescent 345/138 kv Auto-transformer Estimated t Project Cost: $11.0 M Expected IS Date: 18